2930 61st Street
Menomonie, WI 54751
715-283-4422

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Local Reviews
for hudson, wi

Rated 4.7 out of 5 stars based on 3 customer reviews

Nice repair

I called in the morning and they had someone at our house early afternoon, the guy even put little shoe covers on which made my wife happy. Good guy, we are pleased.


Response from Hurlburt Heating & Plumbing:

Thank you for the wonderful review and for taking the time to share your feedback.

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Best Company I've ever used

I've had other companies plumbing work and work on my furnace and air conditioner before but Hurlburt Heating is on a different level. The entire experience was perfect, other service companies could learn from them. I'll tell everyone about them.


Response from Hurlburt Heating & Plumbing:

Thanks for sharing your review with us and the community.

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Recommend!


Response from Hurlburt Heating & Plumbing:

Thanks for sharing your review with us and the community.

  • Overall Experience
  • Quality
  • Price
  • Convenience

Job Locations
for hudson, wi

Jared R.

Jared R. Job Checkin

Replaced damaged draft combustion inducer assembly on furnace after identifying issues with the motor shaft. Performed comprehensive system check including heat exchanger, flame sensor, ignitor, and wiring connections, and replaced air filter. System now operating normally with proper combustion and airflow.

Replaced damaged draft combustion inducer assembly on furnace after identifying issues with the motor shaft. Performed comprehensive system check including heat exchanger, flame sensor, ignitor, and wiring connections, and replaced air filter. System now operating normally with proper combustion and airflow. Replaced damaged draft combustion inducer assembly on furnace after identifying issues with the motor shaft. Performed comprehensive system check including heat exchanger, flame sensor, ignitor, and wiring connections, and replaced air filter. System now operating normally with proper combustion and airflow.

Kegan M.

Kegan M. Job Checkin

Responded to service call for loose kitchen faucet. Upon inspection, determined that the Glacier Bay fast mount system was broken and no longer securing the fixture properly. Provided customer with estimate for complete faucet replacement as repair of existing mounting hardware not feasible.

Responded to service call for loose kitchen faucet. Upon inspection, determined that the Glacier Bay fast mount system was broken and no longer securing the fixture properly. Provided customer with estimate for complete faucet replacement as repair of existing mounting hardware not feasible. Responded to service call for loose kitchen faucet. Upon inspection, determined that the Glacier Bay fast mount system was broken and no longer securing the fixture properly. Provided customer with estimate for complete faucet replacement as repair of existing mounting hardware not feasible.

Scott N

Scott N Job Checkin

Replaced faulty fill valve and flapper in upstairs toilet that was continuously running and had caused overflow damage to the downstairs ceiling. Performed visual inspection of associated plumbing components and water heater system to ensure proper operation after repair.

Replaced faulty fill valve and flapper in upstairs toilet that was continuously running and had caused overflow damage to the downstairs ceiling. Performed visual inspection of associated plumbing components and water heater system to ensure proper operation after repair. Replaced faulty fill valve and flapper in upstairs toilet that was continuously running and had caused overflow damage to the downstairs ceiling. Performed visual inspection of associated plumbing components and water heater system to ensure proper operation after repair.

Jared R.

Jared R. Job Checkin

Responded to no-heat call for aging boiler displaying E3 error code. Diagnostic inspection revealed extensive water damage throughout system including severe corrosion on heat exchanger, damaged sensors, leaking low water sensor, and water damage affecting gas valve and inducer motor. Documented condition with photos showing significant rust accumulation and electrical component deterioration. Prepared comprehensive repair estimate and scheduled comfort advisor to discuss replacement options with customer.

Responded to no-heat call for aging boiler displaying E3 error code. Diagnostic inspection revealed extensive water damage throughout system including severe corrosion on heat exchanger, damaged sensors, leaking low water sensor, and water damage affecting gas valve and inducer motor. Documented condition with photos showing significant rust accumulation and electrical component deterioration. Prepared comprehensive repair estimate and scheduled comfort advisor to discuss replacement options with customer. Responded to no-heat call for aging boiler displaying E3 error code. Diagnostic inspection revealed extensive water damage throughout system including severe corrosion on heat exchanger, damaged sensors, leaking low water sensor, and water damage affecting gas valve and inducer motor. Documented condition with photos showing significant rust accumulation and electrical component deterioration. Prepared comprehensive repair estimate and scheduled comfort advisor to discuss replacement options with customer.

Jared R.

Jared R. Job Checkin

Performed comprehensive furnace tune-up including inspection of heat exchanger via camera, verification of all safety components (pressure switch, limit switches), and testing of operational elements (burners, blower, inducer). Checked gas pressures, combustion air, and cycled system on high/low settings to confirm proper operation. Replaced ejection tubing from condensate pump to drain and installed water leak sensor. System functioning normally after service.

Performed comprehensive furnace tune-up including inspection of heat exchanger via camera, verification of all safety components (pressure switch, limit switches), and testing of operational elements (burners, blower, inducer). Checked gas pressures, combustion air, and cycled system on high/low settings to confirm proper operation. Replaced ejection tubing from condensate pump to drain and installed water leak sensor. System functioning normally after service. Performed comprehensive furnace tune-up including inspection of heat exchanger via camera, verification of all safety components (pressure switch, limit switches), and testing of operational elements (burners, blower, inducer). Checked gas pressures, combustion air, and cycled system on high/low settings to confirm proper operation. Replaced ejection tubing from condensate pump to drain and installed water leak sensor. System functioning normally after service.

Xavier C.

Xavier C. Job Checkin

Investigated customer-reported intermittent gravelly noise primarily audible upstairs while furnace was operating normally. Inspection revealed a heavily soiled furnace filter which was replaced, and identified the humidifier as producing fan noise with a pad requiring replacement. System operation was verified after filter replacement, with recommendations to monitor for noise recurrence. Scheduled follow-up water heater inspection.

Investigated customer-reported intermittent gravelly noise primarily audible upstairs while furnace was operating normally. Inspection revealed a heavily soiled furnace filter which was replaced, and identified the humidifier as producing fan noise with a pad requiring replacement. System operation was verified after filter replacement, with recommendations to monitor for noise recurrence. Scheduled follow-up water heater inspection. Investigated customer-reported intermittent gravelly noise primarily audible upstairs while furnace was operating normally. Inspection revealed a heavily soiled furnace filter which was replaced, and identified the humidifier as producing fan noise with a pad requiring replacement. System operation was verified after filter replacement, with recommendations to monitor for noise recurrence. Scheduled follow-up water heater inspection.

Mike B.

Mike B. Job Checkin

Responded to no heat call for furnace with blinking red light. Diagnosed seized combustion blower motor preventing proper system operation. Attempted to restore functionality but determined replacement necessary. Customer approved repair estimate; return visit scheduled to install new combustion blower.

Responded to no heat call for furnace with blinking red light. Diagnosed seized combustion blower motor preventing proper system operation. Attempted to restore functionality but determined replacement necessary. Customer approved repair estimate; return visit scheduled to install new combustion blower. Responded to no heat call for furnace with blinking red light. Diagnosed seized combustion blower motor preventing proper system operation. Attempted to restore functionality but determined replacement necessary. Customer approved repair estimate; return visit scheduled to install new combustion blower.

Kegan M.

Kegan M. Job Checkin

Diagnosed pressure tank system exhibiting short-cycling (5-6 minute intervals for approximately 10 seconds) with no gauge movement. After isolating the house with the main valve, determined pump continued to activate, indicating a leak on the well side of the system. Customer referred to well company for specialized service.

Diagnosed pressure tank system exhibiting short-cycling (5-6 minute intervals for approximately 10 seconds) with no gauge movement. After isolating the house with the main valve, determined pump continued to activate, indicating a leak on the well side of the system. Customer referred to well company for specialized service. Diagnosed pressure tank system exhibiting short-cycling (5-6 minute intervals for approximately 10 seconds) with no gauge movement. After isolating the house with the main valve, determined pump continued to activate, indicating a leak on the well side of the system. Customer referred to well company for specialized service.

Kegan M.

Kegan M. Job Checkin

Responded to service call for water pressure issues and hot water concerns. Diagnosed and replaced faulty pressure switch on recently installed pressure tank, resolving delayed water flow problem. Inspected water heater and found no error codes present; system was producing adequate hot water during service visit.

Responded to service call for water pressure issues and hot water concerns. Diagnosed and replaced faulty pressure switch on recently installed pressure tank, resolving delayed water flow problem. Inspected water heater and found no error codes present; system was producing adequate hot water during service visit. Responded to service call for water pressure issues and hot water concerns. Diagnosed and replaced faulty pressure switch on recently installed pressure tank, resolving delayed water flow problem. Inspected water heater and found no error codes present; system was producing adequate hot water during service visit.

D S.

D S. Job Checkin

Conducted comprehensive plumbing inspection of bathroom fixtures, focusing on toilet and sink connections. Examined water supply lines, shut-off valves, and mounting hardware for both fixtures, confirming all components are in good working condition with no visible leaks, damage, or deterioration.

Conducted comprehensive plumbing inspection of bathroom fixtures, focusing on toilet and sink connections. Examined water supply lines, shut-off valves, and mounting hardware for both fixtures, confirming all components are in good working condition with no visible leaks, damage, or deterioration. Conducted comprehensive plumbing inspection of bathroom fixtures, focusing on toilet and sink connections. Examined water supply lines, shut-off valves, and mounting hardware for both fixtures, confirming all components are in good working condition with no visible leaks, damage, or deterioration.

Bryson E.

Bryson E. Job Checkin

Completed annual plumbing inspection revealing several maintenance issues requiring attention. Primary concerns include a failing pressure tank, non-functional valves (hot side in main bathroom and basement toilet), missing hammer arresters on washing machine, and deteriorating flappers in master and basement toilets. Provided customer with detailed estimate for recommended repairs and replacements.

Completed annual plumbing inspection revealing several maintenance issues requiring attention. Primary concerns include a failing pressure tank, non-functional valves (hot side in main bathroom and basement toilet), missing hammer arresters on washing machine, and deteriorating flappers in master and basement toilets. Provided customer with detailed estimate for recommended repairs and replacements. Completed annual plumbing inspection revealing several maintenance issues requiring attention. Primary concerns include a failing pressure tank, non-functional valves (hot side in main bathroom and basement toilet), missing hammer arresters on washing machine, and deteriorating flappers in master and basement toilets. Provided customer with detailed estimate for recommended repairs and replacements.

Kegan M.

Kegan M. Job Checkin

Responded to service call for automatic flush valve malfunction in women's restroom. Diagnosed broken flush valve with wires disconnected from motion sensor to solenoid. Restored toilet functionality temporarily, but replacement parts will be required for permanent repair.

Responded to service call for automatic flush valve malfunction in women's restroom. Diagnosed broken flush valve with wires disconnected from motion sensor to solenoid. Restored toilet functionality temporarily, but replacement parts will be required for permanent repair. Responded to service call for automatic flush valve malfunction in women's restroom. Diagnosed broken flush valve with wires disconnected from motion sensor to solenoid. Restored toilet functionality temporarily, but replacement parts will be required for permanent repair.

Bryson E.

Bryson E. Job Checkin

Replaced customer's broken elongated toilet tank with complete new Kohler toilet unit after assessment determined replacement was more practical than tank-only repair. Installed new toilet seat and lid assembly with proper mounting hardware, ensuring secure connection to the bowl. Verified proper function and no leaks before completing service.

Replaced customer's broken elongated toilet tank with complete new Kohler toilet unit after assessment determined replacement was more practical than tank-only repair. Installed new toilet seat and lid assembly with proper mounting hardware, ensuring secure connection to the bowl. Verified proper function and no leaks before completing service. Replaced customer's broken elongated toilet tank with complete new Kohler toilet unit after assessment determined replacement was more practical than tank-only repair. Installed new toilet seat and lid assembly with proper mounting hardware, ensuring secure connection to the bowl. Verified proper function and no leaks before completing service.

Trent L.

Trent L. Job Checkin

Inspected air exchanger system for reported water leakage from insulated ductwork. Found moisture on fresh air intake and stale air ducts with wet areas below. Enabled defrost function that was previously disabled to prevent freezing in cold conditions. Installed additional straps on insulated flex ducts to create proper slope for drainage back to unit. Advised homeowner that these adjustments would be monitored for effectiveness in resolving the persistent leakage issue.

Inspected air exchanger system for reported water leakage from insulated ductwork. Found moisture on fresh air intake and stale air ducts with wet areas below. Enabled defrost function that was previously disabled to prevent freezing in cold conditions. Installed additional straps on insulated flex ducts to create proper slope for drainage back to unit. Advised homeowner that these adjustments would be monitored for effectiveness in resolving the persistent leakage issue. Inspected air exchanger system for reported water leakage from insulated ductwork. Found moisture on fresh air intake and stale air ducts with wet areas below. Enabled defrost function that was previously disabled to prevent freezing in cold conditions. Installed additional straps on insulated flex ducts to create proper slope for drainage back to unit. Advised homeowner that these adjustments would be monitored for effectiveness in resolving the persistent leakage issue.

Doug T.

Doug T. Job Checkin

Conducted plumbing inspection of residential water treatment system. Identified improperly installed water softener drain and recommended replacement of the whole home filter (homeowner supplied). Noted the current Morton water softener from Menards has approximately 3-year lifespan remaining; offered to provide future replacement quote when needed.

Conducted plumbing inspection of residential water treatment system. Identified improperly installed water softener drain and recommended replacement of the whole home filter (homeowner supplied). Noted the current Morton water softener from Menards has approximately 3-year lifespan remaining; offered to provide future replacement quote when needed. Conducted plumbing inspection of residential water treatment system. Identified improperly installed water softener drain and recommended replacement of the whole home filter (homeowner supplied). Noted the current Morton water softener from Menards has approximately 3-year lifespan remaining; offered to provide future replacement quote when needed.