Upon arrival tech was informed that the blank thermostat was for the older system that served half of the showroom. The power was cut off at the disconnects for the condensing units at a request of the customer due to renovations on that side of the showroom. Tech restored power and verified the thermostat powered up. Tech did check on the newer system due to the history of the system. There was some adjustments made to the system and it was operating upon departure.
Tech arrived and replaced 2 compressor contactors, after replacing tech cleared all faults and cycled system both circuits cycled and were running normally but when cycle stop compressor 1 contractor fault appears. Tech started diagnosing using Trane website instructions and found all controls and switches test to specs, tech was unable to find cause of fault code at this time, tech spoke with office regarding issues office is found to discuss and call back with solution. Tech cycled system and found system will run on circuit 2 until issue is resolved.
Tech assured the power was off to the carrier systems due to renovation. Symbio system - found compressor 2 proving and compressor contactor 1 failure faults. Tech acknowledged the faults and tested the system from the app and operated compressor 1 for 10 seconds and then shut off due to contactor failure fault. Compressor 2 was operating only. Faults were acknowledged and checked pressure switches and Discharge temperature sensor and checked good. Pressures were good when compressor 1 was bypassed for testing purposes. Compressor contactor 1 is recommended to be replaced due to the Normally open switch being a challenge at intermittent times. Tech went over the testing process based on Trane website, for proving compressors and it led back to the compressor contactors. Office will be informed of the findings and would need to return with 2 compressor contactors to be safe. Tech acknowledged the faults and had both compressors operating prior to departure and showed the manager on sit
Tech turned disconnect for the system were the renovations were completed on. Technician also turned the disconnect for the side were they are going to start renovating off. 2 systems.
Remove Existing Carrier 2 Ton Split Heat Pump And Install New Trane 2 Ton Heat Pump System With WiFi Programmable Thermostat Remove Non-Operable Duct Detectors And Install New Duct Detectors
— Performed CMA Full Service on 3 Split System Heat Pumps and 1 Twin Split System Heat Pump. — Large renovations in progress for left side of building. — 1 Back Left System - 2024 Trane Split Heat Pump: Left Side Showroom: System has been manually turned off at outdoor disconnect. Left side showroom system not to be operated while renovation is ongoing. System clearly was being operated as renovations were in progress. System may be in need of duct cleaning. Recommend immediate filter change on system once put back in use after renovation. System has been off for an extended period of time and may need a senior to tech to perform a service call to confirm settings and parameters in programming when brought back online. — 2 Right Front System: 2020 Carrier Twin Split Heat Pump: Right Side Showroom: No air filters in place upon arrival. Filter rack has been uninstalled by others. Reinstalled as appropriate. Installed air filters as found on site. — 3 Back Left System - 2006 Carrier
Technician returned to replace adaptor board and 3 pole contactor. Tech replaced and system started up no issues. Tech performed multiple test on system to ensure system is operating properly technician also got multiple pictures of breaker panel and disconnect.
Tech found circuit 1 contactor failed. Technician cleared alert system started both circuits when tech called with thermostat and cir1 would not engage only circuit 2 tech tested all sensors found no challenges. Technician bypassed proven fault and wired directly to contactor. When called y1 compressor would engage eveytime. Tech suspects either proven switch is malfunctioning or add board is due to not sending 24v from board to contactor. Will inform office and follow up.
On arrival, staff reported showroom gets to 78 with setpoint at 71. Also reported break room hot and back/visual room ductwork dripping onto floor. Small Carrier R22 split system was found to have failed R22 compressor on May 9th this year. System still down with disconnect locked out. Tech recommends replacing small R22 split system for break room. Tech ran back room system for an hour. Observed no drips. Tech recommends keeping doors closed as much as possible to prevent outside air humidity from entering back room. 20 ton Trane split system thermostat was satisfied at 71 on arrival. Gave system a cooling call and system started in first stage. Found aux pan full of water, but drain is clear. Found condensate dripping directly off of indoor coil into aux pan. Started pumping excess water from aux pan. System is calling for Y2. Y1 compressor isn't running. Y2 is. Tech acknowledged compressor contactor failure error and cycled line voltage. Both circuits are now running. Found a litt
Upon arrival tech found system with a compressor contractor fault dated for 5/28, the day before last visit. The thermostat was found to be blank, tech found the auxiliary drain pan full and pan switch tripped. Tech removed water from auxiliary pan and cleared fault. System cycled came on and ran with no challenges. Tech installed drain on the auxiliary pan and ran outside the building. Tech collected operating information of system. Tech only seen a few drops of water from air cabinet when unit was cycled off. Tech did find some insulation curled up in corner near drain of air handler. There was some water droplets on the filters, tech lowered blower capacity from 75% to 70% to decrease coil temperature, to help condensation adhere to coil.
-Found system showing diagnostic error for broken blower belt again. -Examined parameters on VFD and found RPM set wrong according to motor data plate. Corrected parameter and observed motor torque readings. Verified findings versus prior RPM settings to confirm this was causing torque readout to go out of spec and cause error code. -Issue with error code should now be resolved. Install supervisor will follow up throughout the week. If problem persists throughout the weekend, install supervisor will schedule a call Tuesday.
Found alert code on the VFD board indicating a “broken belt alarm”. Belt is good and tension as well. Went spoke with our install supervisor about the findings and ended up increasing the tolerance level of the “broken belt” parameter 22-61. Factory setting is 10%. Tech tested the system afterwards in cooling and waited for it to reach set temperature at the thermostat. Indoor blower torque range stayed between 130-140% operating at full speed. System was tested from the thermostats from “off” to “cool” multiple times and system started up without challenges. Covered under install warranty. Split system for the break room is still down for now. Thermostat temp went from 75 to 73 degrees during cooling.
System short cycling upon arrival. Found the smoke detector tripped upon arrival on the new Symbio split system. Check wiring for tightness and reset the smoke detector. System started up without challenges. Smoke detectors do have resistors. System on the other side of the building is also operating. Tech spoke with the install supervisor about the findings and was informed that new smoke detectors are being quoted by Colby, smoke detector on the other older unit is not connected. Tech by passed the emergency stop at the Symbio control board for the time being until the smoke detectors get replaced. Wires hanging from the ceiling were also strapped up and not hanging. Tech noticed the compressor not engaging for the break room and found a tripped breaker at the panel located in The electrical room. R22 Compressor is seized up. Carrier split system is down. Tech wrote the information of the unit on paper and uploaded it on file. Split system for the break room is down for now. Colby w