Larry was a good communicator, and provided context for his recommendations. Thank you!
Response from X-Treme Temp Heating & Cooling, LLC:
It was a pleasure serving you and your family. Thank you for sharing your kind words with us. It means the world to us and to our entire team!
Service performed as expected.
Response from X-Treme Temp Heating & Cooling, LLC:
Thanks for the positive rating on your routine maintenance and repair service.
Turned system on and checked. System did not turn on. Checked the condensate pump, it was not tripped. Installed the overflow switch in the secondary drain pan. There may have been a loose wire. Checked all wires. Started and tested. Adjusted the thermostat several times and the system turned on and off properly.
Checked system. There was no power to the thermostat. There is a condensate pump in the attic next to the unit. When arrived, the blower door was off and the pump was unplugged. Plugged the pump in and it was in alarm due to the tank was full. It pumped the water out properly and it came out of alarm. Checked all the low voltage wires. There is an overflow switch in the secondary pan. The overflow switch is not operating properly, there is no water in the pan and it’s breaking the circuit. The overflow switch needs to be replaced. Removed the wires for the overflow temporarily to get the system running. Checked the charge, the system is low on refrigerant. Added 15 oz R410a to the system. 60*f discharge air. The system is operating properly at this time. Need to order and return to replace the pan switch.
Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps While performing the maintenance we found the compressor amp levels were slightly elevated for a cooler day. Would recommend replacing the unit in the near future due to age and stress on the compressor.
Turned the system on and the burner started, when it was up to temp the blower motor did not turn on, just buzzed. Checked the capacitor. The run capacitor is bad. Replaced the capacitor and the motor started. On start up the start winding is louder then normal, then quiets down. The motor will need to be replaced in the future.
Upon arrival unit was on but not running. We found the firomatic t handle had gone bad and was not letting oil flow to the burner. Replaced the t handle and started and tested the system. Unit is working properly. Recommend having a chimney person come and look at the entryway to the chimney liner.
Installed a new Reillo electric air shutter motor. Started and tested several times. System is operating properly.
Turned the thermostats up and the burner started and stopped. Found the air shutter was spinning and was not stopping at the end switch. Disconnected the motor and taped the end switch closed so it will fire. Cycled the burner several times. Need to order and replace the air shutter motor.
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the air filter. 20x20x1 Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 7.0% o2, 0 ppm, 84.0% efficient System is operating properly. The 6” Tee flue pipe, the metal is starting to get thin and soft in a couple of spots. Recommend replacing before a hole starts to form.
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 5.5%o2, 1 ppm, 86.% efficient System is operating properly. The water heater is showing signs of a leak. Recommend replacing before it leaks water.
Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps
We will drain the system. Cut out and move the Zone 2 flocheck and install a flocheck for zone 3. Fill and purge all zones. Price includes Silver Member discount.
In Middlefield, CT, during a routine HVAC system maintenance, I identified a compromised capacitor affecting the compressor's efficiency. Additionally, a blockage in the condensate drain line was found, posing a risk of water damage and reducing humidity control. The capacitor was replaced with a new unit, and the drain line was cleared of debris, ensuring the system's optimal operation and reliability.
In Middlefield, CT, I am performing comprehensive heating maintenance. Also replacing a faulty thermostat for this customer. All critical components such as air filters and coils were thoroughly inspected and cleaned, improving overall system performance. All checks were made and this client's heating system is prepared for the ongoing season.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.9%o2 20ppm co 0 smoke
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Replaced air filter- 20x20x1 and adjusted the blower belt. Started and checked the safeties. Performed a combustion test. System is operating properly. The blower wheel is dirty and recommend having it cleaned.