340 Quinnipiac Street / Building 33
Wallingford, CT 06942
203-815-6851

Local Reviews
for meriden, ct

Rated 5.0 out of 5 stars based on 45 customer reviews

X-tremely thorough

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Great experience

Quick response to an emergency. Tech was very professional, knowledgeable and courteous.


Response from X-Treme Temp Heating & Cooling, LLC:

Thank you so much for your 5-star review! We will share this with the team to let them know to keep up the amazing work.

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Best Service!

Larry and his entire team are always professional, personable and very responsive. He is transparent when explaining services performed, recommendations and pricing.

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Excellent service

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Excellent

Andrew kicked ass and got me heat back in my house

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Excellent Company and Staff!

You can’t go wrong with Xtreme Temp! They are very professional, discuss everything in detail that has been done, and are very reasonable!

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Excellent service!

Very detailed, informative and answered all my questions.

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Excellent Experience and Service

Professional Service. I highly recommend Xtreme Temp.

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Always quality and friendly service

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Professionalism

Very pleased with the work performed and grateful for letting me know of any possible problems that may arise in the future.

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Excellent service

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Outstanding Work

super job, furnace has NOT run this good since new!! Highly recommend "X-Treme!!

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Excellent service

The technician was respectful, knowledgeable and addressed all my concerns. He promptly arrived and got right to work. He cleaned up after he was finished. I would absolutely recommend this company.


Response from X-Treme Temp Heating & Cooling, LLC:

Thank you so much for this great 5-star review.

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Great Service

Andrew very nice young man and he takes pride in his work

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Excellent Service

Excellent service. Highly trained technician Arrived on time. Professional and courageous. Answered all questions. Highly recommend this company for heating/cooling service!

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Job Locations
for meriden, ct

Larry H.

Larry H. Job Checkin

Performed an A/C pm on (2) systems. Replaced the air filters for the attic system and washed the filters for the ductless system. Blew out the drain lines. Rinsed the condenser coils. Checked the electrical connections, pressures and temperatures. The Fujitsu ductless, 117*f in heat, 47*f in cooling. Systems are operating properly.


Andrew H.

Andrew H. Job Checkin

Washed condenser coil Checked all electrical connections and safeties Blew out drain lines and poured water to ensure proper draining Tested all heads in high heat and cool Checked volts and amps Visually inspected evap coils, blower compartments and filters. Washed all filters with water. All heads were putting out 109-118 degree air in high heat mode and were putting out 45-55 degree air in high cool mode. Unit are operating properly Would recommend cleaning the blower wheel of the head in the first bedroom upstairs.


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was off on reset. Checked the history of the primary control and saw that out of the 15 saved previous runs only 3 lit and the ohms were well over 2000 for all 3. This indicates that the cad cell eye was having a hard time seeing the flame. Checked oil flow and had a lot of air in the oil line. Checked the nozzle and saw it had been dripping. Also saw a large formation of carbon in front of the nozzle assembly indicating the nozzle had been dripping for a while. Replaced the nozzle, cleaned the electrodes and removed the carbon buildup and any oil residue. Bled the oil line again and started and tested the system. Had to cycle on and off multiple times to burn off all excess oil from when the system was not igniting. Started and tested the system. Unit is running at 7.2%o2 40ppm co 0 smoke Recommend getting a maintenance done before the end of the heating season as one has not been done in over a year.


Andrew H.

Andrew H. Job Checkin

Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.7%o2 80ppm co 0 smoke While performing the maintenance we found that the combustion chamber has fallen apart and a section is missing from the bottom. Showed the customer and informed them it may impact the performance of the furnace. While performing the combustion test we found that the o2 increased from 4.3%o2 up to 5.2% when the blower turned on indicating there is a crack in the heat exchanger. Recommend replacing the furnace before any issues arise.


Larry H.

Larry H. Job Checkin

The expansion tank has a spot of the water side of the tank that is starting to leak and bubble the paint. The tank needs to be replaced. Isolated and drained the pressure from the boiler. Removed and replaced the extrol tank. Filled and purged the system.


Larry H.

Larry H. Job Checkin

Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 10.4% o2, 1ppm, 0 smoke, 78.9% efficient System is operating properly. There are (2) Hi-vents that have corrosion on the top of them from a previous leak. Recommend replacing them.


Andrew H.

Andrew H. Job Checkin

Upon arrival water heater was off and valved off. Opened valves to fill the water heater and found that the pressure relief was the cause of the water leak. Once the water heater was full the pressure relief started dripping. Drained water from the system and removed the old pressure relief. Installed the new pressure relief and filled the system back up with water. Started and tested the system. While testing the water heater we found that the aquastat was not sensing the water temperature correctly. When the aquastat was set to 100 the unit would not turn off until the temperature of the water was 125-130. Recommend replacing the water heater instead of the aquastat due to the age of the tank.


Larry H.

Larry H. Job Checkin

Valve off the boiler and drain. Replace the circulator pump. Fill and purge the system. When the system was empty, noticed the pressure gauge was still reading 20 psi. Replaced the pressure/ temperature gauge. Started and test.


Larry H.

Larry H. Job Checkin

Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. While testing the system, the boiler came up to temperature and zone valves opened but the circulator did not turn on. There was 121volts coming out of the aquastat going to the circulator. The circulator is drawing 0amps. The circulator pump is bad and needs to be replaced. The domestic coil gasket has leaked and corroded the steel of the tankless coil and possibly the boiler. The boiler is older.


Andrew H.

Andrew H. Job Checkin

Brushed and vacuumed burner tubes Inspected and vacuumed burner compartment and surrounding area Checked electrical connections and safeties Checked gas pressure Performed combustion test Inlet pressure-7.017 Manifold pressure- 3.019 10.1%o2 22ppm co


Larry H.

Larry H. Job Checkin

Drain pressure from the system. Remove 3 old hi-vents and replace with 3 new hi-vents. Fill system back up with water. Purge all zones of air. Start and test system.


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was off on reset. Upon further inspection found the boiler was plugged internally. Performed emergency cleaning on the boiler. Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 8.0%o2 30 ppm co 0 smoke


Andrew H.

Andrew H. Job Checkin

Upon arrival found the system had air in it and also saw the boiler pressure was around 5. Lightly lifted the arm on the autofeed and the autofeed lest more pressure into the system. Air got into the system when the autofeed never filled the system back up with water when air would leave the system. Bled both zones and got all air out of the system. Boiler pressure when leaving was 20 psi. Unit is working properly. May need to replace he autofeed in the future if it continues to stick and not add water to the system.


Larry H.

Larry H. Job Checkin

Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 7.1%o2, 0ppm, 0 smoke, 81.6% efficient System is operating properly. Removed burner motor and cleaned the blower wheel. There was some cat hair in the wheel. Recommend vacuuming around the area due to fur was on the pipes and on the burner. Don’t want to have issues in the future.


Larry H.

Larry H. Job Checkin

The water heater burner was off on reset. Reset the control and it started then the flame went out. Checked the oil flow, the oil was foamy with air. Checked the oil tank, the level is at approximately 3/4. Checked the oil filter. The filter was dirty but not plugged. Replaced the filter. After replacing the oil filter, checked the flow at the furnace and noticed a lot of air in the line. Bled the line until there was good clean oil at both appliances. Followed the oil line from the tank to the mechanical room, the line sits on top of the concrete, did not see any oil residue or oil spots. The concrete is rough where the oil sits. If there is still an issue with air in the line, recommend replacing the oil line. With the line sitting on the concrete, it can wear a hole a draw in air.