340 Quinnipiac Street / Building 33
Wallingford, CT 06942
203-815-6851

Local Reviews
for hamden, ct

Rated 4.9 out of 5 stars based on 12 customer reviews

Great service

Good job, prompt and informed.


Response from X-Treme Temp Heating & Cooling, LLC:

We are so grateful for your 5-star review. Thanks for sharing your rating with us and the community.

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Good service

All good. Thks

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Very Professional Service!

Very reliable and knowledgeable staff

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Great service

Andrew was a wonderful young man. He was most courteous and very helpful in explaining what was needed to be done on the boiler.

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Great Service

Courteous, on time, efficient , professional

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excellent service!!

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Excellent and prompt

Courteous technician fixed our unit quickly. Great price.

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Very professional service

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Good

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Awesome service

The technician was friendly and professional answered all my questions. The answering personal working the phones are also wonderful. Would highly recommend

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Great service

Andrew was very nice , respectable and polite polite.

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Job Locations
for hamden, ct

Andrew H.

Andrew H. Job Checkin

Performed routine maintenance on a 4-ton central AC system. Cleaned condenser coil, inspected the capacitor, flushed the drain line, and tightened electrical connections. Found compressor amperage running high, so we’ll recheck next visit. Advised client to keep landscaping trimmed around outdoor unit to prevent debris buildup and overheating. System is currently operating within normal specs.


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was on but not running. Turned thermostat up. The unit started to light but a couple seconds after the flame came on it put the flame out. Inspected the flame sensor and found it was very corroded and starting to get thin in some places causing it to not sense the flame. Went to a supply house to get a new flame sensor. Removed the old flame sensor and installed the new one. Also found the air filter was plugged and covered in dog hair. Replaced the air filter with a company supplied one. Started and tested the unit. Unit is working properly.


Larry H.

Larry H. Job Checkin

Installed a new Bradford White electric water heater for a homeowner. Removed the old leaking unit, installed the new tank, and connected the water supply and electrical lines. Checked the pressure relief valve, filled the tank, and tested for proper operation. Ensured the homeowner had consistent hot water before completing the job.


Andrew H.

Andrew H. Job Checkin

Inspected interior of boiler and checked door gaskets Cleaned the condensate trap and filled it with clean water Checked all boiler piping for leaks and corrosion Checked flue pipe and air piping Checked system pressure and controls Inspected and cleaned ignition electrode Checked all boiler wiring connections and safeties Started and tested the system


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was on but not running. Temp in the house was 73 and the thermostat was set to 71. Turned temp up to 76 and unit started up with no issue. Cycled unit on and off multiple times with no issues. Checked all radiators and all of them were getting hot. Compared the thermostat temp to a temp probe and found the thermostat is reading 3 degrees warmer than the indoor temp is. Most thermostats have a 3* temperature variance. The thermostat may be starting to go bad. Adjusted the hi and low limits on the boiler aquastat so the burner will run for longer periods of time. Unit is working properly.


Andrew H.

Andrew H. Job Checkin

Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 7.8%o2 48ppm co 0 smoke When arriving unit was off on reset. Pushed reset button and furnace lit right away. Checked oil flow and had good flow. Checked the igniter and saw the spark was an orange/yellow color indicating it is getting weak. After getting customer authorization we replaced the igniter. Started and tested unit. Unit is working properly.


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was on but not running. Ran hot water and the water heater turned on with no issue. Checked oil flow and had ok flow. Checked the nozzle and found it was dripping with oil on the end cone and in the blast tube. Replaced the nozzle and started the water heater. We found when the furnace turned on while the water heater was running the water heater would turn off. Upon further investigation we found the oil filter by the wall was starting to get dirty and restricting the oil flow. Since the furnace is closest to the filter the majority of the oil was flowing to the furnace and making the water heater turn off. Replaced the oil filter and bled the oil line. Also removed the oil filter from the filter canister by the water heater because the oil filter at the wall is rated for 2 appliances. Started and tested the water heater by itself and when the furnace was running as well. Unit is working properly.


Larry H.

Larry H. Job Checkin

Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 5.7% o2, 0 ppm, 86.3% efficient System is operating properly. There is a cup under the pressure relief valve with a small amount of water/ glycol in it. The valve is currently not leaking and the pressure is at 20psi. If the valve starts to leak more, recommend replacing the pressure relief valve.


Andrew H.

Andrew H. Job Checkin

Disconnected wires for the old zone valve and removed the old zone valve. Installed new zone valve and reconnected all wires. Removed old thermostat from the wall and installed a new Honeywell t4 thermostat. Started and tested the heat in the entry way zone. Unit is working properly.


Andrew H.

Andrew H. Job Checkin

Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 13.5%o2 26ppm co 0 smoke While performing the maintenance we found higher than normal levels of sludge at the oil filter canister. After getting customer authorization we added sludge additive to the oil tank. When taking the flue pipe apart one of the flue pipe 90’s broke apart due to rust and corrosion. Was able to put it back together but the 90 was too rusted to be able to rotate. Had to replace the flue pipe 90. Recommend replacing the remaining sections of flue pipe due to age and corrosion. While performing the combustion test we found the crack in the heat exchanger is slightly larger than last year. Opened the inspection door of the furnace and was able to visually see multiple spots where the sheet metal of the heat exchanger has holes. Showed the customer with an inspection mirror. Recommend repla


Andrew H.

Andrew H. Job Checkin

Removed zone valve and replaced with new one. Installed zone panel and connected all zone valves to the zone panel. Started and tested all zones to ensure proper operation. Bled radiators and made sure all radiators were functioning. While testing zone 3 for the air handler we found that the water was continuously circulating when there was no call for heat but the fan was not turning on. After further investigation we found the freeze stat clamped by the air handler was bad. The freeze stat thought the pipes were cold and was turning on the circulator pump and opening the zone valve. Need to replace the freeze stat.


Andrew H.

Andrew H. Job Checkin

Performed oil pm on oil boiler Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 7.0%o2 30ppm co 0 smoke Performed ac pm on both systems Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps While testing the ac unit in the closet of the front of the house we found that the heat and ac were running at the same time. Upon further investigation we found the zone valve we diagnosed as bad last year hooked up. When we left the property last year we had the zone valve disconnected because it was stuck in the open position and was continuously sending hot water to the air handler. Disconnect


Andrew H.

Andrew H. Job Checkin

Upon arrival unit was off inspected evap coil and air filter and both were good. Poured water down the drain line and found no blockages. Started the system. Air handler and condenser fan turned on but no compressor. Upon further inspection we found the capacitor for the compressor had gone bad and had a terminal shorted out. Replaced the capacitor and the wire terminal for the compressor wire. Started and tested the system. Checked the refrigerant levels and system was working properly. Had 48* supply air when leaving


Andrew H.

Andrew H. Job Checkin

Upon arrival u it was off. Customer stated the oil tank was empty and they got a delivery the other day. Bled oil line and saw some sludge. Checked the nozzle and found heavy carbon buildup on the nozzle and nozzle assembly. Cleaned the carbon buildup and replaced the nozzle. Slightly adjusted the electrodes. Bled the oil line again and started the boiler. Performed combustion test and adjusted the air and fuel. Unit was running at 5.6%o2 45ppm co. Added oil sludge additive to the oil tank and had customer verify the oil fill cap was on the pipe.


Andrew H.

Andrew H. Job Checkin

Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps While performing the maintenance we found the unit was slightly low on refrigerant. After getting customer authorization we added 9 oz R410A bringing the subcooling from 5.2 up to 12