Andrew arrived on time and was courteous and thorough in explaining the work that was needed on our a/c unit. The a/c is working much better now thanks to his fix!
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The service by X-Treme is always performed professionally and done properly.
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Good job, prompt and informed.
Response from X-Treme Temp Heating & Cooling, LLC:
We are so grateful for your 5-star review. Thanks for sharing your rating with us and the community.
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Andrew was a wonderful young man. He was most courteous and very helpful in explaining what was needed to be done on the boiler.
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Courteous technician fixed our unit quickly. Great price.
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The technician was friendly and professional answered all my questions. The answering personal working the phones are also wonderful. Would highly recommend
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Overall Experience
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Upon arrival unit was on but not running. Checked the thermostat and it was turned up and calling for heat. Went downstairs and saw the furnace was not running and the furnace doors were ajar. Removed the top and bottom panels and put the bottom panel on again. Once we adjusted the door the furnace turned on with no issues. The furnace blower door was not fully pressing in on the door switch and was not letting the furnace turn on. Watched the system cycle on and off 5 times. Unit is working properly. Took pictures and measurements for a media filter box. Current filter is 16x25x1
The water heater was off on reset. Reset the control and it started properly, when the furnace turned on, the water heater was loosing oil flow and shutting off. Blew out the oil line going to the u der ground tank. Primed the oil line. Turned the furnace on then the water heater, the water heater was reading 420 ohms and staying steady for 8 minutes while the furnace was on. System is operating properly.
Burner was off on reset. Reset the control and it started. Checked the ohms, the cad cell was reading 1300 ohms which will cause it to go off on reset. Adjusted the cadcell eye and it was reading 540 ohms. Installed a used Beckett primary control to see history and ohms. While the water heater was running, the furnace turned on and 10 seconds later the water heater went off on reset. Replaced the oil filter at the wall. Started and checked operation. It was still doing the same thing. After the furnace was satisfied, checked the oil flow at the water heater and noticed a little bit of air. The oil tank is under ground and can not see the level. The customer had 100 gals added on Dec 9. Recommend having another delivery due to issue.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests While performing the maintenance we found a small amount of water and rust inside the oil filter canister. Recommend getting oil sludge additive to remove any water and sludge buildup. Customer has a space guard 2200 air filter and wants one for ac maintenance
The burner was off on reset when arrived. Reset the control and it started. Checked the oil flow with the water heater on and also with the furnace. Checked the oil filter at the wall, filter is ok. Removed the nozzle assembly and found the nozzle is bad. Replaced the nozzle, started and tested.
Checked both furnaces and thermostats there was no codes on either furnace. Started and tested both several times and they started properly. Checked the program on both thermostats. The 1st fl was set to - less than 90% when it is a 90% 2 stage furnace. Changed the setting to more than 90%. The 2nd fl was set to single stage heat, the furnace is a 2 stage 90% furnace. With the very cold weather early in the morning, the 2nd floor was not keeping up and the cold air was falling down to the 1st floor. The thermostat downstairs was also reading 14% humidity which will make the room feel cold. Recommend installing a humidifier.
Boiler Installation: The property’s aging boiler struggled to maintain consistent pressure and often required manual resets. After determining the system was inefficient and beyond economical repair, I installed a modern, high-efficiency boiler. I updated the zone valves, optimized the circulation pump, checked combustion levels, and confirmed stable heating across all zones.
Autumn HVAC Maintenance: Arrived at the client’s home to perform seasonal autumn furnace maintenance. Inspected and cleaned the burner assembly, heat exchanger, and blower compartment, replaced the air filter, and verified proper thermostat operation. Checked all electrical connections, safety switches, and ignition components to ensure reliable performance for the upcoming cold season. Tested the furnace to confirm strong, consistent heat output. The system is now clean, working efficiently, and ready for winter operation.
Upon arrival unit was on and running. Found oil dripping from the burner. Took the oil pump and oil burner motor off of the burner and cleaned all oil. Removed the nozzle assembly from the blast tube and found oil dripping from the nozzle and oil in the blast tube. Found a large amount of oil covering the nozzle assembly. Inspected oil pump shaft and seal and found a small amount of oil residue but did not see any noticeable leak from there. Inspected the oil line and did not see any leaks. With the burner not leaking a large amount of oil while running it is difficult to pinpoint exactly where the oil is leaking from. After getting customer authorization we went and got a used nozzle assembly to put in and eliminate that as a possible source of the oil leak. Returned to the house and put a new nozzle in and the used assembly and cycled the unit on and off multiple times. After running the unit for a few cycles we found the oil leaking was slightly less than what was happening with the
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 6.1% o2, 26 ppm, 80.6% efficient System is operating properly. Purged all zones of air.
Performed heating maintenance on hydro air handler and gas water heater Brushed and vacuumed burner for the water heater Inspected and vacuumed burner, blower compartments and surrounding area Checked electrical connections and safeties Checked gas pressure Performed combustion test Flushed water heater to remove sediment Replaced air filter
Customer turned the thermostat on and the condenser just hummed. Found the capacitor was bad. Replaced the capacitor, started and checked the pressures. System is operating properly.
Upon arrival unit was off. Checked air filter and it was good. Checked condenser coil and found it was dirty. When the condenser coil is dirty it traps the heat and causes the pressure and temps of the refrigerant to act higher than they really are. Washed the condenser coil to remove the dirt buildup. Checked wiring in the condenser electrical compartment and at the compressor. Found a mouse nest in the compressor jacket. Removed the jacket and the mouse nest. Did not see any damaged or chewed up wires. Checked the condenser for any traces of Uv dye and did not find any. Started and tested the system and found the unit was slightly low on refrigerant. The manufacturer states the unit should have 11* subcooling +/- 3* and the unit was bouncing between 7-9. After getting customer authorization we added 9 oz R410A to the system bringing the subcooling up to 13.6* which is acceptable. Had a 17.5* temp difference between the supply and return before adding the refrigerant and 21* differenc
Performed an A/C pm on (2) systems. Blew out the drain line, replaced the air filter on the 2nd fl, 1st fl was clean. (Customer supplied) Checked and tested the condensate pump. Rinsed the condenser. Checked the electrical connections, checked the pressures and temps. On the 2nd condenser, replaced the suction side schrader due to not seating fully after checking the charge. System is operating properly.
Upon arrival unit was on but the thermostat was satisfied. Turned thermostat down and both indoor and outdoor units turned on. Checked the evap coil and the air filter and both were clean. Checked refrigerant levels and found the liquid pressure was very high. Found the condenser coil was very dirty. When the condenser coil is dirty it raises the refrigerant temp and pressure, also making it harder for the unit to cool properly. After getting customer authorization we chemically cleaned the condenser coil. After cleaning the coil we found the unit was slightly low on refrigerant. The manufacturer calls for a subcooling of 7* at 85* outside but the unit was only at 3* subcooling. After getting customer authorization we added 7 oz R410A to the system bringing the subcooling up to 9. Unit is working properly. Had 10* temp split when arriving and 17* split when leaving.