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Great Company ! Jonathan was so professional on a Sunday Emergency call to help me out . This my go to company for my HVAC needs .
Response from Hydes Air Conditioning:
Thank you so much! We are grateful for your business and your recommendation.
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Always great customer service from start to finish!!! I always highly recommend Hydes!!
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He was very professional and polite. He is welcome to my house anytime he’s such a nice guy.
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Thor was very friendly and polite. Explained everything in detail. Great technician.
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Equipment iced up on arrival, evaporator coils iced up. Performed diagnostic on equipment and found equipment very low on r22 refrigerant. Equipment in very poor condition well past life expectancy. Not able to read data plat on outside equipment possibly 2004 model equipment. Advised equipment has leak in refrigeration system. R22 refrigerant no longer manufactured, and refrigeration coils are no longer available. Highly recommend replacing equipment and update equipment to 2025 refrigerant for long term solution. Option 1 is to replace partial system-condenser and evaporator coils. Option 2 replace complete system. Attention below attached 2 options below.
Performed annual maintenance in heat on a train package unit followed Sequence of operation Changed filter checked amps voltage capacitors limit switches safety switches working at range cleared burners cycled burners cleared condensation line unit is working to manufacture specification in heat, recommend blower wheel cleaning organic growth all over blower wheel
Emailed ductless proposals and left messages.
Installed new thermostat and tested operation. Verified sequence of operation is working properly at this time
Re sent estimate to turn condenser around
The services provided include the installation of complete ducting, register cans, new tstat wire and flex for the restroom exhaust fans. This installation encompassed the integration of supply and return plenums through the curb, along with the installation of new flexible ducting featuring wyes and supply return cans to ensure optimal airflow and efficiency in the system. The customer will call the office to schedule the package unit install once the roofing is done.
Scope of Work: • Relocate existing condenser unit. • Electrical will be run in conduit alongside refrigerant lines. • Trenching and burial of lines will cover approximately 10 linear feet. Notes: • This estimate covers only the relocation of the condenser and associated trenching. • All electrical will be installed in conduit per standard practices. • This quote does not include responsibility for code compliance or inspection-related liabilities required by the city. It is the responsibility of the homeowner or general contractor to ensure all work complies with applicable codes and to obtain any required permits. We Will need a condenser pad
Service Type: Demand Service – No Cooling Date: Aug 22 2025 System Info: 2013, 3.5 Ton Condenser Unit ⸻ Issue Reported: Upon arrival, the client reported that the system was unable to maintain set temperature during the peak heat of the day. Thermostat was set to cool at 77°F, with an indoor temperature reading of 80°F. ⸻ Diagnostics Performed: • Followed a sequence of elimination to diagnose issue. • Air Filter: Checked and found to be in good condition. • Electrical Components: • Checked capacitor, contactor, fan motor, and compressor. • Measured amperage and voltage. Findings: • The condenser fan motor was found to have visible oil marks around the housing, indicating wear. • Motor was pulling above the manufacturer’s rated amps, confirming the part was failing. • Other components showed signs of age but were still operational. ⸻ Recommendations & Client Approval: Discussed findings with client and recommended replacing the following original components for improved r
Downsized 15-50 quad breaker down to a 15-40 to match max rated breaker size for condenser.
Dropped off permit and inspected equipment to verify it is up to code. Need to return to replace square d quad 15-50 beaker down to a 15-40 square d quad breaker. Client does not need to be home but will need access to side gate to get to electrical panel.
2021/ 4 ton Preformed a semi annual cooling service on Lennox split system. Replaced two 20x30 and 20x20 filters/ceiling. Cycled equipment followed, cooling sequence of operation checked refrigerant and temperature split checked capacitor, fan motor, compressor, amps and voltage. Secured and clean electrical connections at condenser and fuse box. Thermostat checked out OK. Cleared condensation line from outside. Rinsed condenser coil. Cooling equipment checked out operational at this visit Recommendations Equipment LRA 94 A Currently pulling 118 A Spoke with client about adding a hard start kit to help compressor on start up
Removed and replaced exhaust fan in hallway bathroom.
Service Call – No Cooling Client Complaint: Upon arrival, the client reported that the system temperature fluctuates and, at one point, was unable to maintain the set temperature. Diagnosis & Actions Taken: • Set the thermostat 10°F lower than the current setting to force system operation. • Performed full system check and Refrigerant pressure • Went to retrieve digital gauges for a more accurate reading. Upon return, noticed the condenser fan was not operating. • Inspected wiring and connections — checked Molex connector — issue traced to a faulty condenser fan motor. • Went to the shop to pick up a replacement condenser fan motor. • Replaced the condenser fan motor. • Checked capacitor, running amps of fan motor and compressor, and refrigerant charge. • Verified proper temperature split. Outcome: System is now operating properly and within manufacturer limits. Next Steps: This call is paused. Will follow up with the client later today to ensure the system continues to per