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Wes did a thorough investigation of our furnace issue and ordered the needed parts.
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Evans called my tenant and made after hours appointment with out stating that there was a $60 fee for an after hours appointment. The tenant would have been ok with waiting until Tuesday.
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Couldn’t have asked for a better technician. Shalik was a joy to have in our house.
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Overall Experience
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Shalik was very thorough and friendly Awesome job
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Technician arrived on time. Friendly and knowledgeable. Worked quickly and efficiently and made me aware of issues he found. Estimates to repair are being supplied.
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Andrew was on time, polite, efficient and thorough. I will definitely use this company for further service for my furnace and air conditioner l
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Good service. He explained everything clearly. Nice guy to deal with. Very professional.
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The technician was friendly and did a great job, we are very pleased all round! 😀
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Wesley was very thorough explaining things as he went. He completed the inspection and cleaning of the furnace and did a thorough job pinpointing the Freon leak in a very unusual spot.
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They were polite and f
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Furnace Maintenance: Water damage noted under the ventor motor, starting to part, reaching out to office for quote. Collector box p trap has a hairline fracture, added silicone to mend will quote out new one. Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Humidifier tested and inspected for proper operation. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently.
Furnace Maintenance: Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently.
Comfort club Weil mclain boiler maintenance
Lennox furnace maintenance Cleaned and inspected furnace Inspected all electrical equipment Tested gas pressure Tested drainage Tested safeties Performed combustion analysis Furnace is clean and working well. No problems came up during testing. Replaced 6670 filter Replaced humidifier pad
Lennox furnace maintenance Cleaned and inspected furnace Inspected all electrical equipment Tested gas pressure Tested drainage Tested safeties Performed combustion analysis Furnace is clean and working well. No problems came up during testing. Replaced 6670 filter. Inspected humidifier pad. Found it to be clean and not needing replaced.
Furnace Maintenance: Upon start up the ventor motor is audible loud, showing its age, still operating okay though. Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently.
Furnace Maintenance: Adjusted high stage gas pressure (3.9"wc) to meet manufacturing requirements of 3.5"wc. Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently. Susie and Layla
Furnace Maintenance: Replaced the media filter with x6670 (16x25x5) Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently. HRV: Removed and cleaned the core. Vacuumed each section, followed by vinegar polish. System is operating well.
**Air Conditioner Service Call** **Work Performed:** - Responded to concern of evaporator coil freezing on an air conditioner installed in 2024. - Verified all furnace and fan functions — both operating normally with a clean filter. - Checked refrigerant levels and found them low. - Inspected system and observed an oil stain near the outdoor Schrader valve, suggesting a possible refrigerant leak. Tightened schrader valves. - Added leak sealant as a precaution and charged approximately 3 lbs of refrigerant to restore proper system levels. - System now operating normally. **Results:** - Possible leak at the outdoor Schrader valve or elsewhere in the system.(tightened, and inspected, no leak suspected after system recharge) - System stabilized after refrigerant top-up and sealant uv dye injection. **Recommendations:** - In the spring, schedule a full maintenance and leak search to confirm if the Schrader valve was the source of the leak or if further repairs are required.
Furnace Maintenance: Tightened the bolts connected tto the ventor motor flue exhaust. Media filter was in good condition so kept it as is. Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently. Noticed some built up corrosion on the hot water tank, hot pipe.
**No Heat Service Call – Keeprite Furnace (2006)** **Work Performed:** - Responded to a no heat call for a 2006 Keeprite furnace. - Found the inducer motor not operating and no voltage being sent from the circuit board. - Removed the inducer motor to inspect internal condition — motor was not spinning but the blower wheel is in good condition. - Verified inducer motor functions properly when 120V was applied directly, confirming the circuit board is not providing power. - Circuit board also not sending voltage to the igniter and producing irregular clicking noises; tapping the board caused random activation sounds. **Results:** - Circuit board determined to be faulty and the source of the no heat issue. - Collector box interior found to be muddy upon inducer removal. - Client expressed interest in having the collector box cleaned. **Recommendations:** - Circuit board replacement is required. - If collector box cleaning is performed, replacement is recommended due to proprietary gask
Furnace Maintenance Recommend new/updated plug-in carbon monoxide detector for the basement. Flushed the condensate P-trap and drain lines to maintain clear, efficient flow. Checked pressure switch tubing to ensure reliable performance. Cleaned and polished the flame sensor for optimal ignition. Ran full diagnostics to confirm the system is running smoothly and efficiently.
Furnace repair - Daikin furnace not heating. Upon arrival, un able to see flashing liht on control board because the circuit board wiring was blocking it. Took apart furnace and began testing. Ventor motor turning on, Ignitor lighting but no ignition. Tested 26v going to the gas valve. Verified gas valve switch was on. Traced wires to the .10 w.c pressure switch the condensation line. Switch not closing. Inspected and found a blockage in the hose. Blew out condensation line and re tested. System fired up and began operating as intended. Perform combustion anaylsis to ensure system is fully operational and safe …see photos. Tested all other components, everything is in good working order. System is safe and fully operational.
Installed nest thermostat. Had to take G wire and use it as common as there were only 4 wires. Explaines they would lose functionality of the “fan on” setting. They did not use this anyways with the old thermostat. After completion of installation tested heating and cooling to make sure both worked correctly.
Evans Premier Furnace Installation