Elijah was wonderful. After he finished he explained everything he did in detail, and answered all my questions. Very thorough.
Response from Garner Heating & Air Conditioning Inc:
We are pleased to know your experience with us was a good one!
Tech arrived on time and was very professional. Great customer service.
Zach did a great job of checking every little nook and cranny of our two systems. He highlighted and photographed all the critical parts and let us know of any areas of concern. Never pushy or rushed.
Called first, on time, courteous, respectful, answered questions; what more can you ask for?
Service rep was very friendly and efficient. Took time to answer my questions thoroughly.
Outstanding, as alway! Elijah is very knowledgeable & professional.
Baker was great! As a Vietnam War Veteran, I was glad to have an Army Veteran as my AC technician. Baker was competent and responsible.
Performed semiannual maintenance on one heat pump cooling system. Inspected all Performance, Mechanical and Safety Systems. Verified everything was operating within manufacture’s specifications for operation. Everything is working at this time.
I made sure to rinse out both heat pump condensers and also clear both drains. During my evaluation I noticed the following: both condenser fan motors have extreme wear and/or are leaking oil, the master bedroom system has a weak capacitor, and the main house system has a pitted contactor. I brought all of this to the attention of the customer and gave her a few options. She elected to have me perform the work detailed in my top option. This option includes replacement of the condenser fan motor for the main system and the master bedroom system. Also includes replacement of the contactor on the Main system and replacement of the Capacitor on the master bedroom system. I collected for the work and Matt assisted in the work. Replaced both motors and also replaced the contactor on the main system and the capacitor on the master system. I tested both units once the repairs had been performed and everything is working properly. Systems are in working order at completion of
Performed semiannual maintenance on one straight electric cooling system. Inspected all Performance, Mechanical and Safety Systems. I flushed and treated the primary drain line and cleaned the outdoor condensing coils. In addition, I also changed out the high voltage wire nuts to a bigger size (orange to red), to help prevent overheating of the wires. Verified everything was operating within manufacture’s specifications for operation. Everything is working at this time.
Performed semiannual maintenance on two heat pump cooling systems. Inspected all Performance, Mechanical and Safety Systems. Flushed and treated the primary drain lines, cleaned outdoor condensing coils, and removed all leaves and debris from base of condenser. Verified everything was operating within manufacture’s specifications for operation. Everything is working at this time.
Replaced indoor evaporator coil. Replaced coil drain pan. Replaced liquid line filter dryer. Rebuilt primary and secondary drain. Cleared and verified drain operation. Resealed coil door with mastic. Pressure tested and pulled a vacuum on the copper line set. Weighed in refrigerant charge to meet manufacturers specifications.
Performed semiannual maintenance on two heat pump heating systems. Inspected all Performance, Mechanical and Safety Systems. Verified everything was operating within manufacture’s specifications for operation. Customer mentioned that his drain came undone from the exterior wall penetration. I added some new PVC to the drain outside to give it some support against the ground, so it drains farther away from the foundation of the house. Everything is working at this time.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. Air handler and blower wheel are both clean. Low voltage control wiring was tightened. Drain line was cleared and treated. Condenser coil clean. Electrical disconnect is in good condition. The condenser fan motor is also in good condition. Condenser capacitor is within value and the refrigerant charge is good. No major issues were found, and the system was running at the time of departure.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. The air handler and blower wheel are clean. System sterilizers are operational. Drain line was cleared and treated. The condenser fan motor is in good condition. The capacitor for the condenser fan motor is below value. The contractor is in good condition as well. The refrigerant charge is good, and the system is running normally. Surge protection for the condenser and air handler are both operational. Condenser coil was cleaned. Options for repair were presented and they chose to have the condenser capacitor replaced today. I replaced the capacitor on the condenser and treated the inside of the cabinet with JS insecticide. The system was running at the time of departure. No other major issues found.
Performed semiannual maintenance on two heat pump heating systems. Inspected all Performance, Mechanical and Safety Systems. Attic HVAC System: On the indoor air handler that is located in the attic, I found lots of oil residue on the coil piping. I used my electronic leak detector and soap bubble leak detection solution and found a leak along the coil piping. I also checked the refrigerant charge of the R-22 system and found it to be low Entry Way Closet HVAC System: I flushed and treated the primary drain line and verified all buildup and gunk exited the outside drain exit next to the condensing unit. Also verified the system was operating within manufacture’s specifications for operation. Everything is working at this time.
nstalled 3 Ton Carrier Heat pump and Air Handler. Installed Ecobee Pro Thermostat. Transitioned to existing Supply Plenum. Sealed Return Chase with mastic air lock. Rebuilt and insulated condensate drain line. Installed ss2 safety float switch. Cleared and verified drain operation. Pressure tested system with nitrogen and pulled a vacuum on the line set. Replaced disconnect and whip for outdoor unit. Tested and Verified system charge was at manufacturers specification.
Performed semiannual maintenance on one system. Condensation lines cleared/treated, and float switch is working. The air filter has been changed with homeowner supplied filter. Amp draws are within manufacture specs. Condenser coil has been cleaned. The system is operating properly at this time
Performed semiannual maintenance on one straight electric cooling system. Inspected all Performance, Mechanical and Safety Systems. Changed out one filter provided by Mr. Charles. Flushed and treated the primary drain line. Verified everything was operating within manufacture’s specifications for operation. Everything is working at this time.
Arrived to find the system off. Located new position where customer wanted the thermostat moved to. Ran new wire to location. Moved thermostat and reattached wire to thermostat and air handler. Cycled system on to confirm unit is operating properly.
Performed semiannual maintenance on one heat pump cooling system. Inspected all Performance, Mechanical and Safety Systems. Did note that the indoor coil is extremely rusted and corroded. I used my electronic leak detector to inspect the coil for any refrigerant leaks and at this time none were present. This will require close monitoring to ensure refrigerant levels stay within the manufacturer’s specifications. Flushed and treated the primary drain line and changed one 16x25x4 Honeywell filter. Verified everything was operating within manufacture’s specifications for operation. Everything is working at this time.
Installed Carrier furnace and Carrier heat pump for a dual fuel system. Installed Ecobee Pro thermostat. Installed propane conversion kit. Transitioned to existing return plenum. Built new supply plenum and sealed all connections with mastic. Replaced secondary drain pan. Rebuilt and insulated primary and secondary drain lines. Cleared and verified primary drain operation. Installed SS2 and SS3 safety float switches. Ran new low voltage wire to condenser. Pressure tested and pulled a vacuum on the copper line set. Weighed in charge to meet manufacturers specifications.