4720 Industrial Access Rd.
Douglasville, GA 30134
770-445-8923

Local Reviews
for alpharetta, ga

Rated 5.0 out of 5 stars based on 3 customer reviews

Great Service

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  • Overall Experience
  • Quality
  • Price
  • Convenience

Amazing customer service

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Job Locations
for alpharetta, ga

Brad  N.

Brad N. Job Checkin

DCM9 complete; AC; (8) 20x20x2, (4) 20x25x2, (3) 16x25x2, (1) 20x25x1, (1) 16x25x1, (1) 16x20x1, (1) 10x45x1 replaced (2) Washable filters cleaned. All systems are cooling, most units were still on Heat mode, tested systems and returned them to Heat mode.. Outdoor temperatures were a little low for proper testing procedures but refrigerant pressures and temperatures were appropriate for indoor and outdoor conditions. Kitchen unit is cooling, system was extremely low on refrigerant, added 4 lbs of R22 refrigerant. Compressor runs, then binds, shuts down and restarts and repeats the sequence. System cooled the kitchen from 95* to 78* during location maintenance.


Rob  S.

Rob S. Job Checkin

DCM9 complete; AC; (8) 20x20x2, (4) 20x25x2, (3) 16x25x2, (1) 20x25x1, (1) 16x25x1, (1) 16x20x1, (1) 10x45x1 replaced (2) Washable filters cleaned. All systems are cooling, most units were still on Heat mode, tested systems and returned them to Heat mode.. Outdoor temperatures were a little low for proper testing procedures but refrigerant pressures and temperatures were appropriate for indoor and outdoor conditions. Kitchen unit is cooling, system was extremely low on refrigerant, added 4 lbs of R22 refrigerant. Compressor runs, then binds, shuts down and restarts and repeats the sequence. System cooled the kitchen from 95* to 78* during location maintenance.


Cody C.

Cody C. Job Checkin

Upon arrival no heat in meeting room, heat strip contactor was broken pictures attached*. Replaced contactor with approval. Smoke detector tripped unit on and off for about 30 minutes until all dust was burnt of heat strips. Strips were running continuously for over 20 minutes satisfied at 72 degrees. System is operating properly at this time


Cody C.

Cody C. Job Checkin

DCM1 service 1 of 2 Heat completed changed (1) 20x20x1 filter, tested system operation’s everything is operating properly at this time attached is Heat maintenance checklist.


Brad  N.

Brad N. Job Checkin

Call for no heat in the lobby, on arrival temperatures were set to 80 reading 65, went onto the roof and checked operation and system was starting up and fired up, let system run for a 1hr and checked temperatures in multiple locations in the lobby and was reading 70 and matched the the thermostat readings, checked 1 of the hallway units that is Heat strips only, it is a 6.8 kw it is energizing and doing everything that it can. This location needs 2 techs each time.


Rob  S.

Rob S. Job Checkin

DCM9 complete, Heat; (8) 20x20x2, (4) 20x25x2, (3) 16x25x2, (1) 20x25x1, (1) 16x25x1, (1) 16x20x1, (1) 10x45x1 replaced (2) Washable filters cleaned. (1) AX46, (1) AX54, (1) A39, (1) A50 changed. Systems are fully functional with the following exceptions. RTU #1 ( Server/office ), : Straight AC; indoor fan blower motor has seized and will no longer spin. Blower motor photo attached RTU #3 ( offices ) : Gas valve fails to open. Input pressure on gas valve 24 in WC. Gas valve max pressure is 1/2 psi or 14 in WC. Gas regulator has failed. 3/4 in pipe diameter Photo attached System #6 ( Kitchen ) : System is approximately 4 lbs low on R22, pressures are low on both high and low sides. Superheat is extremely elevated. Indoor metering device is a piston while the outdoor fan has a low ambient kit that is keeping the system from freezing. System is 27 years old Request replacement quote for System #6 and RTU #1. Request repair quote for RTU #3 and RTU #1


Brad  N.

Brad N. Job Checkin

Check Robs invoice.


Rob  S.

Rob S. Job Checkin

Arrived to water damaged sheetrock in women’s bathroom attached to main lobby. Leak is not related to A/C units located on roof


Rob  S.

Rob S. Job Checkin

Tested both systems in heat and reset smoke sensor. Repeated until system stayed in heat without tripping sensor


Rob  S.

Rob S. Job Checkin

Identified faulty wiring at splice for reversing valve wire. Repaired wire and tested system. Functions as designed


Rob  S.

Rob S. Job Checkin

Completed 1. Sealed return plenum 2. Properly connected 8in duct to boot at daughter’s room 3. Properly connected Master Bedroom 6in duct to trunk line 4. Installed high velocity registers in Master Bath / toilet 5. Cleaned trash from behind furnace 6. Added damper to master closet / toilet duct and reduced airflow 7. Tested system to ensure proper system airflow; diagnostics attached. System was left on Med-Hi fan speed, TESP : .75 CFM : 881


Keith D.

Keith D. Job Checkin

1. Clean debris from backside of furnace 2. Remove 6” duct from master bedroom on 10” duct: inner liner not connected 3. Connect supply duct in daughters room (new 8” added) outer liner not connected 4. Seal inside of return box at bottom of furnace 5. Needs a 10x6 (master bath) and 10x4 (master toilet) high velocity registers) 6. Check charge levels of ac system due to adjusting blower speed from high speed to medium high Robb is designated for this project


Dobbs Technician A.

Dobbs Technician A. Job Checkin

Remodified upstairs ductwork to a zoned system. Upsized 4 duct runs. Installed new 6” supply and new 8” return. Installed new supply plenum and new return plenum. Installed customer supplied thermostats


Cody C.

Cody C. Job Checkin

Helped with install


Cody C.

Cody C. Job Checkin

Completed DCM 9: Service 4 of 4 filter change, AC, bill out $667.50 - - AC; (8) 20x20x2, (4) 20x25x2, (3) 16x25x2, (1) 20x25x1, (1) 16x25x1, (1) 16x20x1, (1) 10x45x1 replaced, (2) Washable filters cleaned. (1) AX46, (1) AX54, (1) A39, (1) A50 checked