Installed a new Rinnai direct-vent heater with a new sediment trap and gas flex line. Performed a leak check at 8.5 in. w.c. for 3 minutes; no leaks present. Fired the appliance and verified it is operating properly at this time. Removed and disposed of the old Empire heater.
Arrived on site to diagnose no heat on propane boiler. After our initial inspection, we found that the spark igniter had some soot buildup on it.mwe cleaned it off and boiler started right up. When boiler started there was a very loud subwoofer like sound. We provided an estimate to do a tune up so we could dig deeper into the cause of the noise. It was accepted. We started by turning the gas off and pulling the burner tubes out. We found that they were dirty and had a lot of debris built up inside of them and the burner compartment. We wired brushed the burners and vacuumed out the compartment. We then inspected the heat exchanger which looked good. We put the burners back into place and connected pilot tube. Checked for gas leaks using bubbles. Hooked up manometer and checked gas pressure when boiler kicked on. Pressure was good and the subwoofer-like sound went away after we cleaned the burners. Performed a combustion analysis and checked for CO leaks. Analysis was good and no CO
Replaced the outdoor spigot and installed a new shutoff valve due to the existing sillcock continuously dripping and being original to the 50-year-old home. The old unit was removed, copper piping was cut and prepared, and a new press ball valve was installed with new pipe hangers placed every 4 feet in the work area. Installed new Type L copper piping from the valve to a new 10” Legend sillcock, securely mounted with weather-resistant screws and a rubber gasket to ensure a watertight seal. Water was restored to the home and all work was tested with no leaks present and the system operating properly at this time. Also discussed a partial repipe of the remaining kitchen drain line; however, the customer elected not to proceed at this time due to the complexity of the project.
For this visit, we completed the installation of the DAB booster pump. Homeowner had a new outlet installed near pump location allowing proper operation of pump. During the previous visit, the check valve was installed on the incorrect side of the pump, and due to time constraints, it could not be relocated at that time. Today, we repositioned the check valve correctly and added a new shutoff valve on the outlet side to allow easier future maintenance. We adjusted the pump pressure to 55 PSI, set the water heater expansion tank accordingly, and tested the system for proper operation. No leaks were observed at the time of departure.
Arrived onsite and removed the existing 5/8” copper gas line from the regulator. Installed a new 3/4” black iron manifold and ran a 1/2” copper gas line to the Modine heater. Leak checked at 8.5 in/wc for 3 minutes, no leaks present. Installed a thimble on the interior wall. We did not have the vent adapter on hand, so we will need to return to complete the installation. We will call to schedule the follow-up visit. 12/3/25 installed thimble in exterior wall and vent. Checked c.o. levels, no leaks present. Adjusted manifold pressure to 10 in/wc and verified operation, system is working properly at this time.
12/1 We found that the existing electric water heater had failed and was no longer supplying reliable hot water. We recommended replacing it with a new 65-gallon hybrid water heater to restore dependable performance and improve the home’s overall energy efficiency. Upon arrival, we shut off the home’s water supply and drained the existing water heater before removing it. We reset the concrete blocks to create a level base, then set and leveled the new 65-gallon hybrid unit using shims. We installed a new mixing valve, vacuum breaker, and hot and cold shutoff valves. The electrical connection was tied into the existing circuit, upgrading the cover sleeve to liquid-tight conduit to ensure a code-compliant waterproof seal. Both hot and cold lines were connected to the existing 3/4” copper piping, and the failed gate valve was removed. The water was turned back on and the unit was filled; once full, power was restored and the system was confirmed to be heating properly. A new condensate
Looked at replacing Empire wall heater with Rinnai direct vent heater
-The existing pressure tank has failed due to a ruptured internal bladder and age-related deterioration. We recommend replacing the unit with a new 32-gallon pressure tank to restore consistent water pressure and improve overall system efficiency. -The kitchen drain line was found to have a failed fitting and improper pipe pitch, resulting in poor drainage. Due to limited access, we will replace the affected drain line and correct the slope within the attic to ensure proper flow and prevent future leaks or backups. Completed Work: The rubber tee fitting on the vent line was removed and replaced with a new PVC 90° fitting. The vent line serving the kitchen was previously capped; the bathroom vent line was confirmed to be properly pitched and supported at 4-foot intervals. -The existing drain line entering the kitchen cabinet wall was cut and capped flush with the wall. The section of drain piping below the floor was also capped, and the line was cut further back to allow for proper ada
Well System Upgrade Summary: -Following an inspection of the existing well system, it was determined that the current piping is outdated and lacks adequate filtration. To address these issues, we have completed significant system upgrades to improve water quality, reliability, and pressure throughout the home. Scope of Work: Well Pump and Pressure Tank: -Attempted to reuse and repipe the existing jet pump mounted on the 32-gallon well pressure tank. -Relocated the 32-gallon pressure tank to the location of the previous 20-gallon tank. -Replaced the piping from the existing well shutoff using new 1” copper, properly secured to the wall. -Installed a new tank tee assembly with boiler drain, pressure relief valve, and pressure gauge. -Routed piping to accommodate the new sediment filter and installed shutoff valves. -After multiple attempts to prime the system, the existing pump was found to have failed internally (motor and impeller). -Installed a new Goulds ½ HP well pump connected to
Installed dishwasher and washer dryer in Royalton Vermont