I am very happy for the duct cleaning service provided by Adon Complete. They provided lots of details, explanations, suggestions they provided and they did great work. I would recommend for duct cleaning.
Overall Experience
Quality
Price
Convenience
Overall Experience
Quality
Price
Convenience
Performed a complete heating system maintenance and inspection on 2 2020 Gas system. Inspected and tested all electrical components and safety controls on the indoor unit; all components tested within manufacturer specifications. On both units. Verified system temperatures: return air temperature measured at 71°F; supply air temperature measured at 110°F and risining. The down stairs unit was at 115F and 81 return. Confirmed air filter was recently replaced by client; filter size is 20 x 25” x 4”. I visually inspected the outdoor units The outdoor unit was in good condition Confirmed system was operating properly and heating upon departure. System Status: Operating normally at time of service.
1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested for gas leaks 6. Tested functionality and cleaned flame sensor 7. Tested functionality and cleaned pressure switches and ports 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Tested functionality and visually inspected surface igniter 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. All is well with normal heating cycle. Adjusted aprilaire fresh air intake to 15 from 8 minutes per hour. Blower wheel and evaporator is clean. Surge protection installed on equipment working as intended. Unit in good working order upon departure
Dryer Vent Cleaning, preformed work and presented before and after pictures of results. I preformed a 2 system heat maintenance on 2023 communicating Trane gas furnaces. I tested all electrical and safety components on each system. All tested within manufacturer specifications. I changed both filters at the time of inspection. 20x25x4 and 16x25x4. Temperature being supplied downstairs was at 109 degrees and 73 return. Upstairs was 106 and 68. I proceeded outside to visually inspect the outside units. While visually inspecting I noticed each system did not have any surge protection on the system. Surge protection cause be beneficial to add just in case of a lightning strike and/or surges in power. I provided estimates to have the surge protection installed. Units were heating upon departure.
Preformed 3 system heating maintenance 2014 gas. Tested all electrical components and safeties on each of the units. All tested within manufacturer specifications. We changed all filters 20x25x4(2) and 16x25x4. We did find that the master bedroom blower wheel could benefit from a good cleaning, also found on the upstairs unit and down stairs unit that both could benefit from a duct and plenum box cleaning. Units were cooling upon departure.
1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Rinsed condenser unit to promote heat exchange 16. Inspected heat strips for functionality Found loose wire to heat strips made sure to secure this wire and tested heat strips and found no issues. Air quality is superb. Unit in good working order upon departure.
Heating preventative maintenance on two gas systems from 2019 using air filters 20*25*1 (main unit) and 16*25*1 (master bedroom). During our inspection we checked temperatures, checked electrical connections and components, measured the attic insulation, changed air filters with ones customer provided, performed a gas leak search on both units, cleaned safety sensors, and inspected the systems for dirt buildup. Overall the systems are heating properly and safe. We did notice the systems don’t have surge protection and informed the customer but he isn’t interested at this time. Customer is on a monthly payment vip agreement.
Blower motor replacement Arrived at our clients home to confirm the diagnosis for the intermittently failing blower motor. I was in the process of diagnosing the motor but was unable to replicate the issue. Jody requested I replace the motor and take care of the issue for her. Once the motor was replaced I proceeded to test and inspect the refrigerant pressures for the system. Everything measured within manufacturer specifications. We turned the thermostat down to 76º and we discussed how the unit will run for a while before satisfying the desired set piping. The system is cooling on departure.
We installed new txv and filter dryer. We didn't need any refrigerant
Arrived on site, found alerts on thermostat for low pressure lock out. Reset power on system and it came on. Measured refrigerant pressures and found there to be a restriction on the low side. Upon further inspection, we found that some of the TXV capillaries are touching the liquid line. Upon removing the sensing bulb and warming it up pressures returned to normal. We removed the capillaries from the liquid line and adjusted the bulb position to 2 o’clock from 3 o’clock. Pressures started to look better after this, but still indicating a restriction in the system. Informed homeowner that we will need to replace this txv under parts and labor warranty.
Arrived on site, and found water dripping out of emergency drain line. Upon inspecting the attic unit, I found water in the drain pan. Outside I found the drain line was run into an irrigation box a little too deep. Upon lifting the drain line a little out of the water, water immediately began draining out. Made drain line adjustments to shorten the pvc going into the drainage box to allow overflow. 20 degree split across the coil was measured with a 53 degree supply. Extensively tested drain line to ensure the line was clear and found it to be draining fine at this time. Unit in good working order upon departure.
Arrived on site for quality control check. Started inspection of indoor unit, found unit to be putting out a cold 55 degrees with more than a 20 degree temperature split. Inspected wiring connections and found no issues. No obstructions of the indoor coil or air leaks. Tested drain lines and found a small issue with the negative pressure of the unit sucking up water. Added a cap to prevent this from happening. Checked refrigerant pressures and found them to be in range. Outdoor unit is leveled properly. Tested float switch to ensure proper operation of safety features and found no issues. Inspected line set and found it to be free of leaks or kinks. Unit is in good working order upon departure.
Scope of Work – Upstairs System Upgrade The existing upstairs HVAC system is currently a 3-ton unit. This project will involve upgrading the upstairs system to a 5-ton TRANE system to increase cooling capacity. System Components: • Outdoor Condenser: 5-ton rated TRANE condenser. • Evaporator Coil: Upgraded to meet full 5-ton capacity. • Gas Furnace: Upgraded to an 80,000 BTU TRANE gas furnace. Ductwork: • If any additional ductwork modifications are required to meet 5-ton airflow requirements, this will be the customer’s responsibility. • This scope covers only the system change-out to achieve the 5-ton capacity for the upstairs unit. Warranty Coverage: • 10-Year Manufacturer Mechanical Warranty – Provided through TRANE. • 2-Year Labor Warranty – Provided through JB Associates.
Upon arrival spoke to clients wife about the hot spots in the house. She showed us which rooms were hotter than others in the upstairs. One being the daughters bedroom and the other being sons bedroom. We proceeded up into the attic space and adjusted the dampers on the two supply ducts. We proceeded to do the cooling maintenance for all three systems. We check all electrical components on the inside units. All tested within manufacture specifications. We did notice that all three could benefit having a safety float switch added to the main drain lines. The upstairs and down stairs units ducts are dirty. Provided estimates for duct cleanings wi5 7 additional returns along with 3 float switches. Master bedroom ducts were not dirt at the time of the inspection. Master bedroom unit filter was changed. upstairs and downstairs filters were not available to change. Size20x25x4 We proceeded to the outside units. We test all electrical components on each of the units. The maters bedroom uni
Preformed cooling maintenance for 2 systems. Tested all electrical components on inside and outside units. All tested within manufacture specifications. Tested run and start amps on outside units. The down stairs unit could benefit from having a hard start kit installed to help get the amps down on units start up. The upstairs unit start and run amps are testing within manufacture specifications. Rinsed both outside units coils. Changed filters for client. Treated main drain lines on both units with total c. Units are cooling upon departure. 521 ELECTRONIC HARD START 189-227 UF 170-277V 1 HP AND UP HARD STARTS ARE USED TO GIVE COMPRESSORS A HIGHER STARTING BOOST OF CURRENT WHEN NEEDED TO START. 521 compressor saver comes with a manufacturer warranty of 2 years from date of installation.
Came out today for QC visit on new install. Started inside at t-stat (Trane) turned system down to check over unit. System is level all wiring is good no error codes. Getting over 20 degree temp split. Drain line is draining at this time. System is clean and operating as designed. Outside unit is level all electrical components are good and tight. All components are operating as designed. Added 1 lb of 454b. Pressures were within manufacturer specifications. Found supply temps a bit high which prompted further investigation. Upon closer inspection I found the liquid line slightly kinked. Assured homeowner that we would be out this evening to address the issue and get it taken care of. Also performed maintenance on both other units. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Ch