824 S Central Expressway, Suite 100
Anna, TX 75409
903-482-4900

Local Reviews
for celina, tx

Rated 5.0 out of 5 stars based on 2 customer reviews

Awesome service, again!

  • Overall Experience
  • Quality
  • Price
  • Convenience

Awesome service, fabulous price

Couldn't have asked for anything better. Charles was on time, honest, respectful, clean, worked quickly and accurately. Awesome service.

  • Overall Experience
  • Quality
  • Price
  • Convenience

Job Locations
for celina, tx

Shelby S.

Shelby S. Job Checkin

Upon arrival, I found the breaker for the outdoor unit. I checked the compressor to ground and I ohmed it out. I inspected the wires for the compressor and found no exposed wire. I took a start amp reading and it it pulling 137 amps on start up before it trips. I unwired the compressor to see if the condenser fan motor would work. It did in fact work. I installed a hard start kit and got the start amps to 98amps, but it still tripped. I swapped the main breaker at the the panel to test if the breaker was bad. It still tripped, and this allowed me to determine that the compressor is bad. We will need to reach out to century in the morning to get an ETA for the compressor.


Matthew C.

Matthew C. Job Checkin

Arrived at clients house, client stated unit stopped cooling around midnight. Client changed filter. Indoor fan was on and running but no cool air was present. We proceeded outside and found that the capacitor was dead and not allowing the compressor to start. Offered Tubro200X and generic capacitor replacements. Client decided to have neighbor replace the capacitor.


braydenwebb@hotmail.com

braydenwebb@hotmail.com Job Checkin

1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser unit to promote heat exchange System


Shelby S.

Shelby S. Job Checkin

I performed a single system cooling maintenance on a 2020 gas carrier system. I checked amps, capacitor, filter, electrical, drains, and cleanliness. The system could use some duct cleaning and blower cleaning. Dust build up can cause the compressor to fail, evaporator coil to leak, and the blower motor to go out. The system currently only has an emergency pan float switch and with the current drain configuration is basically useless. I propose that a in line float and a blow out valve. These items will allow the detection of clogging to be faster and allow the homeowner to clear it. The capacitor was beginning to read weak and I offered a replacement under warranty and a turbo200. The customer approve the turbo200. I installed it and tested the unit for proper operation. 5 year warranty TURBO200 MULTI USE CAPACITOR 2.5-67.5 MFD 370 - 440V SIMILAR TO A BATTERY, CAPACITORS HELP START MOTORS BY STORING CURRENT. A DAMAGED CAPACITOR CAN DAMAGE THE MOTOR IF NOT SERVICED. REGULAR MAIN


Shelby S.

Shelby S. Job Checkin

Performed 3 system cooling maintenance. Systems are from 2016 and are gas. Basement unit is hardly used. I checked amps, capacitors, filters, electrical, drains, cleanliness, and safeties. The systems are performing well with some needed protections and cleanings. The main unit and master bedroom units have some build up in the duct work that could lead to excessive dust build up on the internal parts: blower motor and evaporator coil. This could cause damage to the evaporator coil, blower motor, and compressor. The units do not have surge protection. The units are 2016 with a possible 1 year left of warranty. The compressor needs to be protected due to EPA guidelines that would lead to system replacement if failure occurs.


Shelby S.

Shelby S. Job Checkin

Performed single system cooling maintenance on a 2021 zoned gas system. I checked amps, capacitor, filter, electrical, drains, cleanliness, rinsed the unit, and safeties. The system overall is cooling well with some needed recommendations. The indoor unit has an air leak causing water to accumulate in the emergency drain pan. This can lead to the pan rusting and forming a water leak hazard. The primary drain line does not have a float switch or blow out valve. This serve as a protector against water damage associated with drain line clogs and allows it to be cleared by the home owner. The outdoor unit has a capacitor that is just under its specification rating. I recommend replacement of the capacitor before it fully fails leaving the home owner in the heat. The compressor is pulling high amps upon start up. If the amps continue to go up, there may be irreversible internal damage done to the compressor. Also, it was o served that the unit currently does not have any surge protection. S


Jacob P.

Jacob P. Job Checkin

I returned to our clients home to install the replacement defrost control board. I first undid the bypass I had left over night. I then was able to properly replace the board. Once replaced I asked our client to turn on the thermostat to cool and ensured the unit was running properly before leaving. I also showed our client pictures of potential entry point that rodents use to get into the unit and we discussed using copper wool to help reduce rodent activity.


Jacob P.

Jacob P. Job Checkin

I arrived at our clients home for the main unit not cooling properly. Our client said it was working fine but when they returned home it was not coming on outside. I proceeded outside and began testing the equipment. I found evidence that rodents had compromised the low voltage wires for the outdoor unit. I did some further testing and found the outdoor control board to be compromised. It was not sending the correct power to the contactor. I contacted Trane and they informed me the system is no longer under warranty. The board is in stock and we will pick it up tomorrow and return to complete the full repair. Our client elected to have me bypass the board as a temporary fix today and turn on the air conditioning only. I also covered some of the compromised spot of the wire inside the heat pump. The unit is cooling on departure.


Jacob P.

Jacob P. Job Checkin

I arrived at our clients home for the downstairs unit not cooling properly. Our client noticed the unit was on inside but not keeping the set temperature on the thermostat. I proceeded into the attic and verified the unit was on and sending the signal for the outdoor unit. I proceeded outside and began testing the equipment. I found the capacitor to be failed and I found the thermostat wires to the high pressure switch to be chewed up by a rodent. I showed my findings to our client and we discussed repair options. They elected to bypass the pressure switch as a temporary fix but understand a pressure switch is needed to protect the compressor from overheating and high pressures. They also elected to replace the capacitor today. Once repairs were made and wires secured I tested the system to ensure it was cooling properly. I did rinse the downstairs unit to also reduce stress from the over system performance. I did send an estimate for a replacement high pressure switch and also indo


braydenwebb@hotmail.com

braydenwebb@hotmail.com Job Checkin

1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 13-14 degrees measured. Lower than expected 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser unit to promote heat exchange Low temp split. Took refrigerant pressures and found everything to be normal. 4T unit cooling 2350 sqft. Undersized unit may be causing temp split and txv missing jacket.


Cesar  O.

Cesar O. Job Checkin

Performed a 3 system spring maintenance ( heat pump). Tasks performed. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked refrigerant pressures. 7. Checked compressor amp draw. 8. Checked condenser fan motor amp draw. 9. Inspected / replaced return filter. 10. Inspected return plenum for debris/ dirty. 11. Inspected evaporator coil. 12. Inspected blower motor/ blower wheel,,,north/ south side of the house units are very dusty recommended a blower cleaning,,,there’s an older unit that cools/ heats the upstairs,, it’s not working properly , homeowner is aware and he’s ok with it not working properly,, he said he never uses it. 13. Checked blower amp draw. 14. Measured temperature differential . 15. Inspected drain lines. 16. Washed condenser unit.


Shelby S.

Shelby S. Job Checkin

I installed new Honeywell damper motors to the upstairs and downstairs zones. Tested them multiple times to ensure that they were closing fully when not calling for cooling. I confirmed that both dampers are opening all the way when it is calling for cooling. The zones are performing properly.


Shelby S.

Shelby S. Job Checkin

Upon arrival, I found the evaporator coil frozen due to air flow issues. It was determined that both, upstairs and downstairs, dampers are not springing open. I tested them to ensure that the internal damper was working properly and that it was only the motor that has failed. I collected a deposit for the work. We will need to order 2 Honeywell dampers. I fixed the dampers to be open and instructed the customer to wait until about 9pm to turn it back on. This will allow time for the evaporator coil to thaw and be able to cool again.


braydenwebb@hotmail.com

braydenwebb@hotmail.com Job Checkin

Replace leaking gas valve


braydenwebb@hotmail.com

braydenwebb@hotmail.com Job Checkin

Customer stated all was well with regards to normal unit operation. I started by changing the air filters on on both units. Blower motor amps were within range. Treated drain lines to prevent future blockages. Measured a 18 ° split on both units. Upon opening up the upstairs unit, I began to smell gas. After further inspection, I found the gas valve to be letting gas out of the orifices. Continuing to the outdoor units, both capacitors were testing within range, however, both contactors were testing high, but within range. Notified customer That these will need to be replaced in time, but it is not urgent at the moment. I wash both condensers to promote heat exchange and prolong the life of the unit. Both units in good working order upon departure. I also shut off the gas to the upstairs unit to prevent further leaking.