Frank was awesome in explaining what was wrong and documented everything with pictures. He was not trying to sell me on everything little thing that could be done, But was helpful in explaining what really was broken and needed to be fixed soon or today. He was honest, respectful, kind and went out of his way to make the experience fantastic. I highly recommend him and his company. I was also extremely pleased and excited that the day I called I got someone out to fix the problem that day. That was impressive.
Am so appreciative of the quality of time and expertise that went into the installation. Beginning with my initial call that was answered on a Saturday night followed by a Sunday consultation and Wednesday installation, Everyone with Adon provided exceptional customer service. The owner is fully involved and truly wants to do a great job for the customer. Am also pleased to support a local business vs a behemoth company where only sales matter. Many thanks to everyone at Adon for their kindness, assistance, professionalism and quality of service.
Quick response, friendly and professional. Didn't feel rushed or pressured. I would use this company again and will recommend them to everyone I know.
Very thorough, professional and clearly explained. Highly recommended.
Adon was a wonderful company to work with. They were quick, helped to explain things, took their time to figure out the problem, and gave their honest opinions on what options we had to fix the problem. I would recommend them to anyone.
Frank was fantastic! He made sure we understood everything and answered all questions throughout the entire visit. He went above and beyond to ensure our units were serviced and that everything looked great.
A blessing to know a company that hires honest and dependable employees
I couldn’t be happier with the service provided by Alex. They were willing to price match a quote from another company and Alex went above and way beyond to take care of our system and even trouble shooting an issue that wasn’t his problem. He wanted to make sure everything was perfect before he left. Additionally, it’s rare to find someone so professional in both their appearance and customer interaction and someone who communicates so well. He really explained everything clearly and you could tell he takes pride in his job and work ethic. I can’t say enough nice things about him. He even honored the agreed upon price even though I know he could have charged us way more for the time he spent. It was so refreshing to meet someone so honest and friendly. Thanks Alex and thanks Adon!!!
Found system was turned off at thermostat. Homeowner explain to me as we were walking in that there was no air movement when you turn the system on. Checked for proper wiring of low voltage wiring at thermostat/air handler/outdoor unit. Made a call for cooling from the thermostat …outside system came on but no blower motor. Provided a call for just fan and still no blower motor running. Diagnostics on air handler/blower motor. Found 3/4 HP 230volt blower motor has failed. Dirty blower motor wheel with debris build up. Drain line/system not retaining water and is draining properly into upstairs bathroom sink. Non operating refrigerant freestanding pressure is good. (R410A) Missing one locking refrigerant cap. 70/7.5 capacitor is weak. Compressor Start up overloaded past manufacturer specifications. Also found that the high pressure switch wasn’t connected and reconnected. Made recommendations for repairs on critical failures to system. System left off in all modes on thermostats and
I arrived at our clients Home for the unit not cooling properly. I immediately proceeded into the attic and did a visual inspection of the equipment. I found a copper line going into the evaporator coil to be frozen. And subsequently there is water dripping into the secondary drain pan. I proceeded outside And found the outdoor compressor to be frozen over. I tested electronics on the outdoor condenser and found the contactor to be near failure as well. I went back inside and opened the evaporator coil and found it to be a complete block of ice. While in the attic, I also inspected the blower motor, it had oil all over itself indicating that it was also near complete failure. I shared all my finding with our client and we attempted to put the unit in heat mode to melt the unit. I let it run but it reached thermal limit due to the hot nature of the home. I sat with Stephanie and we discussed repair vs replacement options. She requested various full system replacement options and we a
I found the primary drain clogged and the system without a filter. I told the tenet that they need to get a filter ASAP. 20x25x4. This system was not installed the best. I cleared the drain line and vacuumed out the pan. The system needs major cleaning and I provided options to address the issue. Customer only wanted me to clear the drain.
Upon arrival, I found the breaker for the outdoor unit. I checked the compressor to ground and I ohmed it out. I inspected the wires for the compressor and found no exposed wire. I took a start amp reading and it it pulling 137 amps on start up before it trips. I unwired the compressor to see if the condenser fan motor would work. It did in fact work. I installed a hard start kit and got the start amps to 98amps, but it still tripped. I swapped the main breaker at the the panel to test if the breaker was bad. It still tripped, and this allowed me to determine that the compressor is bad. We will need to reach out to century in the morning to get an ETA for the compressor.
- Found faulty/failed thermostat for zone one/downstairs. - System currently draining properly and hasn’t retained water. - pulled common wire on zone board/ damper two…to finish diagnostics. - Checked filter/ 20x25x2 / clean / points correct direction - Checked all electrical components as well as refrigerant charge. - System currently functioning cooling properly, except for downstairs zone due thermostat needing to be replaced. Homeowner said he would replace his own thermostat. Instructed him that if he chooses to do this himself to turn off the main power in the attic to the indoor equipment so not blow any fuses or cause any other damage. - System cooling and draining functioning properly upon departure.
1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser unit to promote heat exchange Customer complained of humidity around 60%. Measured sufficient temperature on supply for dehumidification. Could be due to stress on the unit very dirty outside coil. Advised customer to adjust dehumidification settings on nest app to improve dehumidification. Capacitor was testing right on the edge of manufacturer specs. E
I arrived at our clients home for a 2 zone, single system cooling maintenance inspection. I began outside by checking and testing the electrical components to the condenser unit. The capacitor is beginning to fail and the contactor tested at 20 ohms, This is its maximum limit. The compressor was also starting at 153 amps. I then rinsed the outdoor coil from all the debris it had collected. Once washed the compressor started up at 94 amps. Still high but within range. I then went into the attic and treated the drain line. Measured the temperature drop and tested the blower motor. Everything passed inspection in the attic. I showed my findings to our client and we discussed adding a Hardstart kit to help keep the start amps in range and replacing the contactor on the outdoor unit to make sure it doesn’t fail in the middle of summer. He requested that we send an estimate and discuss the options with his wife. The unit is cooling on departure.
1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser unit to promote heat exchange Found both emergency drain pans full of water. Upon further inspection we found that both drain lines are tied together and clogged. CLEAR DRAIN BLOCK - USING NITROGEN ONLY LEVEL 2 CONDENSATE DRAIN LINES NEED TO BE CLEANED OR THEY CAN CLOG WITH ALGAE AND DEBRIS Includes shop vacuuming when necessary and 1 PVC Coupling Al
I performed a 2 system cooling maintenance on 2 gas systems. I checked amps, drains, cleanliness, electrical, filters, and safeties. When operation the systems are cooling good. I found that the drains are tied together and clogged. This is resulting in the downstairs thermostat going off periodically. During inspecting the indoor units, I found that the blower motors on both systems have bearings that are completely worn out. The upstair’s blower motor is filthy adding stress to the motor. The downstairs is starting with higher amps than what is recommended and the capacitor on the compressor side is reading under the manufacturer recommended rating. I offered a new capacitor and a hard start kit. Also, I provided an option for an electrical rebuild for the downstairs outdoor unit. I could not get the drains to clear. I referred the customer to a plumber and told him that we could set the systems up with condensate pumps.
No cool- One system down flow R22 system converted to R421A. Found thermostat intermittently failing and not communicating with equipment. Ran diagnostics on all electrical components and refrigerant charge. High voltage wiring conduit wasn’t connected properly at disconnect for outdoor equipment. Missing insulation on suction at outdoor equipment. Blower motor has significant amount of build up/debris. System is low of refrigerant. System has drop in replacement refrigerant (R421A) used in place of R22. Recommend replacement of entire system due to refrigerant loss and other repairs needed. Did not have replacement Honeywell thermostat on service truck….. running to office to pick up inventory then to return to install new thermostat. Client elected to replace her existing system and install a new heat pump. We applied for financing with John Browder. Finance was approved. We will contact Jean with eta for new system install. We will include new thermostat wire to outdoor and indoo
Arrived on site customer complained of theater room getting too warm and daughters bedroom getting too cold. Adjusted airflow as best we could to push more air to theatre and slightly less to daughter’s room. Closed off damper to upstairs main area with thermostat. May need an additional supply and larger return to accommodate customers preferences. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser uni
REPLACE WARRANTY STANDARD TXV VLV 1 - 5 TON INCLUDES ALL SHIPPING AND MANUFACTURERS PAPERWORK
I performed a single system cooling maintenance on a 2017 straight cool system. I checked amps, capacitors, filters, electrical, drain, cleanliness, and safeties. The system is performing well besides needing a little touch up on the evaporator coil. I provided an option to perform a no rinse coil cleaning.
Second opinion diagnostics on 12 year old 410A upflow system. Found that outdoor and indoor coils are extremely dirty and need a deep clean to stop the icing of the coils. There is a small leak in evaporator coil where the thermal expansion valve meets coil (brazed). Electrical components on the condenser did test within the manufacturer specifications. We did find the that the break in the indoor unit was bypassed and had rust issues from moisture. Filter was completely wet and falling apart. We did replace the filter. Provided estimates for repairs and a new system. Unit was off upon departure.
Performed single system cooling maintenance on a 2012 RTU. The system is a heat pump. I checked amps, capacitor, filter, electrical, drains, safeties, and cleanliness. The system had burnin present on the contactor and the capacitor was reading weak on the compressor side. I replaced both parts and the system is cooling good with a 18 degree temperature drop.