824 S Central Expressway, Suite 100
Anna, TX 75409
903-482-4900

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Local Reviews
for frisco, tx

Rated 5.0 out of 5 stars based on 7 customer reviews

Great service

Adon has a great process when it comes to scheduling and communication. They were very professional and gave a great price to do maintenance on our system. I would use them again.

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Very knowledgeable

The service tech was extremely informative and spent a good amount of time going over our systems.

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HVAC Inspection

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Great service

Was very impressed with the professional work performed at my home by Frank today.

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Great Service

Through, safe and informative by Alex.

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Great service

Very helpful and arrived on time ,late on a saturday night.

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Great Service

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Job Locations
for frisco, tx

Brayden W.

Brayden W. Job Checkin

1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Tested capacitor and contactor (outdoor electrical) 15. Rinsed condenser unit to promote heat exchange 16. Tested emergency heat and found no issues 17. Tested for gas leaks 18. Tested functionality and cleaned flame sensor 19. Tested functionality and cleaned pressure switches and ports 20. Tested igniters No issues at this time all is running well with system. Noticed there was no surge protection on any of the units. Search pr

1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Checked compressor amp draw.
7. Checked condenser fan motor amp draw.
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Inspected blower motor/ blower wheel.
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.
14. Tested capacitor and contactor (outdoor electrical)
15. Rinsed condenser unit to promote heat exchange
16. Tested emergency heat and found no issues
17. Tested for gas leaks
18. Tested functionality and cleaned flame sensor
19. Tested functionality and cleaned pressure switches and ports
20. Tested igniters

No issues at this time all is running well with system. Noticed there was no surge protection on any of the units. Search pr 1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Checked compressor amp draw.
7. Checked condenser fan motor amp draw.
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Inspected blower motor/ blower wheel.
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.
14. Tested capacitor and contactor (outdoor electrical)
15. Rinsed condenser unit to promote heat exchange
16. Tested emergency heat and found no issues
17. Tested for gas leaks
18. Tested functionality and cleaned flame sensor
19. Tested functionality and cleaned pressure switches and ports
20. Tested igniters

No issues at this time all is running well with system. Noticed there was no surge protection on any of the units. Search pr

Brayden W.

Brayden W. Job Checkin

1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Inspected / replaced return filters 7. Inspected return plenum for debris/ dirty. 8. Inspected evaporator coil. 9. Inspected blower motor/ blower wheel. 10. Checked blower amp draw. 11. Measured temperature differential from supply to return. 20 degrees measured. 12. Tested capacitor and contactor 13. Tested electric heat and found no issues Noticed decent amount of dust and debris on condenser coil. Recommend chemical wash to improve efficiency in cooling. Unit in good working order upon departure.

1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Inspected / replaced return filters
7. Inspected return plenum for debris/ dirty.
8. Inspected evaporator coil.
9. Inspected blower motor/ blower wheel.
10. Checked blower amp draw.
11. Measured temperature differential from supply to return. 20 degrees measured.
12. Tested capacitor and contactor
13. Tested electric heat and found no issues

Noticed decent amount of dust and debris on condenser coil. Recommend chemical wash to improve efficiency in cooling. Unit in good working order upon departure. 1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Inspected / replaced return filters
7. Inspected return plenum for debris/ dirty.
8. Inspected evaporator coil.
9. Inspected blower motor/ blower wheel.
10. Checked blower amp draw.
11. Measured temperature differential from supply to return. 20 degrees measured.
12. Tested capacitor and contactor
13. Tested electric heat and found no issues

Noticed decent amount of dust and debris on condenser coil. Recommend chemical wash to improve efficiency in cooling. Unit in good working order upon departure.

Shelby S.

Shelby S. Job Checkin

I found that the motor is in the early stages of failure. This is likely due to its increase usage. The system is zoned, and the fresh air will operate when either zone is active. The suggested route to repair is replacement of the fresh air unit.

I found that the motor is in the early stages of failure. This is likely due to its increase usage. The system is zoned, and the fresh air will operate when either zone is active. The suggested route to repair is replacement of the fresh air unit. I found that the motor is in the early stages of failure. This is likely due to its increase usage. The system is zoned, and the fresh air will operate when either zone is active. The suggested route to repair is replacement of the fresh air unit.

Matthew C.

Matthew C. Job Checkin

Demand call/heat preventative maintenance on two gas systems from 2011 using air filter 20*25*1 which customer did provide today to change. Demand call was for the upstairs system not cooling and having water drip out the emergency line over the garage. Upon a visual inspection the system had an “E312” error code indicating that there was lack of airflow. I checked the air filter and found it to be caked and not allowing proper airflow through the machine causing it to start building frost which led to an excessive amount of water going into the drain pan which drains outside. I took the air filter out and the machine sounded like a drowning victim, the error code cleared after a few seconds. I put the system in ac mode and let it run for 15-20 minutes, the system didnt produce an excessive amount of water because it wasn’t freezing up and I was getting 53 degrees coming out of the vents. On the maintenance I checked electrical connections and components, cleaned safety sensors, i

Demand call/heat preventative maintenance on two gas systems from 2011 using air filter 20*25*1 which customer did provide today to change. 

Demand call was for the upstairs system not cooling and having water drip out the emergency line over the garage. Upon a visual inspection the system had an “E312” error code indicating that there was lack of airflow. I checked the air filter and found it to be caked and not allowing proper airflow through the machine causing it to start building frost which led to an excessive amount of water going into the drain pan which drains outside. 
I took the air filter out and the machine sounded like a drowning victim, the error code cleared after a few seconds. I put the system in ac mode and let it run for 15-20 minutes, the system didnt produce an excessive amount of water because it wasn’t freezing up and I was getting 53 degrees coming out of the vents. 

On the maintenance I checked electrical connections and components, cleaned safety sensors, i Demand call/heat preventative maintenance on two gas systems from 2011 using air filter 20*25*1 which customer did provide today to change. 

Demand call was for the upstairs system not cooling and having water drip out the emergency line over the garage. Upon a visual inspection the system had an “E312” error code indicating that there was lack of airflow. I checked the air filter and found it to be caked and not allowing proper airflow through the machine causing it to start building frost which led to an excessive amount of water going into the drain pan which drains outside. 
I took the air filter out and the machine sounded like a drowning victim, the error code cleared after a few seconds. I put the system in ac mode and let it run for 15-20 minutes, the system didnt produce an excessive amount of water because it wasn’t freezing up and I was getting 53 degrees coming out of the vents. 

On the maintenance I checked electrical connections and components, cleaned safety sensors, i

Shelby S.

Shelby S. Job Checkin

Client is interested in upgrading thermostats, filtration, and air quality. I informed him that we will need some time to properly price the dehumidifier for the downstairs system. I provided pricing for 824 thermostats. These would go best with the equipment that is in the home. I provided pricing for T6 pros, surge protection, filter upgrades, and maintenance.

Client is interested in upgrading thermostats, filtration, and air quality. I informed him that we will need some time to properly price the dehumidifier for the downstairs system. I provided pricing for 824 thermostats. These would go best with the equipment that is in the home. I provided pricing for T6 pros, surge protection, filter upgrades, and maintenance. Client is interested in upgrading thermostats, filtration, and air quality. I informed him that we will need some time to properly price the dehumidifier for the downstairs system. I provided pricing for 824 thermostats. These would go best with the equipment that is in the home. I provided pricing for T6 pros, surge protection, filter upgrades, and maintenance.

Brayden W.

Brayden W. Job Checkin

Arrived on site for dryer vent cleaning and heating maintenance. Homeowner stated all was well with regards normal unit operation to his knowledge proceeded with heating maintenance as scheduled. 1.;Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested for gas leaks 6. Tested functionality and cleaned flame sensor 7. Tested functionality and cleaned pressure switches and ports 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Tested functionality and visually inspected surface igniter 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. Observed both blower wheels had a large amount of dust on them. This creates drag on the motor, causing it to work harder and ultimately shortening the lifespan. I would recommend cleaning both blower wheels

Arrived on site for dryer vent cleaning and heating maintenance. Homeowner stated all was well with regards normal unit operation to his knowledge proceeded with heating maintenance as scheduled.

1.;Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Observed both blower wheels had a large amount of dust on them. This creates drag on the motor, causing it to work harder and ultimately shortening the lifespan. I would recommend cleaning both blower wheels Arrived on site for dryer vent cleaning and heating maintenance. Homeowner stated all was well with regards normal unit operation to his knowledge proceeded with heating maintenance as scheduled.

1.;Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Observed both blower wheels had a large amount of dust on them. This creates drag on the motor, causing it to work harder and ultimately shortening the lifespan. I would recommend cleaning both blower wheels

Brayden W.

Brayden W. Job Checkin

Arrived on site for heating maintenance on carrier two system 2017-2016 furnaces. Homeowner stated all was well with regard to normal unit operation to his knowledge. Proceeded with scheduled heating maintenance. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested for gas leaks 6. Tested functionality and cleaned flame sensor 7. Tested functionality and cleaned pressure switches and ports 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Tested functionality and visually inspected surface igniter 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. Noticed large amount of noise coming from inducer motor on downstairs unit. Made slight adjustment to induce her housing, and the noise went away altogether. This leads me to believe that t

Arrived on site for heating maintenance on carrier two system 2017-2016 furnaces. Homeowner stated all was well with regard to normal unit operation to his knowledge. Proceeded with scheduled heating maintenance.

 1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Noticed large amount of noise coming from inducer motor on downstairs unit. Made slight adjustment to induce her housing, and the noise went away altogether. This leads me to believe that t Arrived on site for heating maintenance on carrier two system 2017-2016 furnaces. Homeowner stated all was well with regard to normal unit operation to his knowledge. Proceeded with scheduled heating maintenance.

 1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Noticed large amount of noise coming from inducer motor on downstairs unit. Made slight adjustment to induce her housing, and the noise went away altogether. This leads me to believe that t

Shelby S.

Shelby S. Job Checkin

Returned to install 4 surge protectors and an ecm blower motor. I needed a 4 leg belly strap to mount the motor. This strap was not a perfect match for the existing holes. I had to do a complete remount of the motor ensure it was centered and operational. I collected via check for the remaining amount.

Returned to install 4 surge protectors and an ecm blower motor. I needed a 4 leg belly strap to mount the motor. This strap was not a perfect match for the existing holes. I had to do a complete remount of the motor ensure it was centered and operational. I collected via check for the remaining amount. Returned to install 4 surge protectors and an ecm blower motor. I needed a 4 leg belly strap to mount the motor. This strap was not a perfect match for the existing holes. I had to do a complete remount of the motor ensure it was centered and operational. I collected via check for the remaining amount.

Jesse V.

Jesse V. Job Checkin

Arrived on site for 4 system heating maintenance. Homeowner stated all was well with normal unit operation to her knowledge. Discussed surge protection with the homeowner to protect the hvac equipment. Proceeded with maintenance as scheduled. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested for gas leaks 6. Tested functionality and cleaned flame sensor 7. Tested functionality and cleaned pressure switches and ports 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Tested functionality and visually inspected surface igniter 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. Upon testing the media room unit, it was found that the blower motor was not working. Further testing revealed that the motor was receiving signal from the con

Arrived on site for 4 system heating maintenance. Homeowner stated all was well with normal unit operation to her knowledge. Discussed surge protection with the homeowner to protect the hvac equipment.  Proceeded with maintenance as scheduled. 
1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Upon testing the media room unit, it was found that the blower motor was not working. Further testing revealed that the motor was receiving signal from the con Arrived on site for 4 system heating maintenance. Homeowner stated all was well with normal unit operation to her knowledge. Discussed surge protection with the homeowner to protect the hvac equipment.  Proceeded with maintenance as scheduled. 
1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested for gas leaks
6. Tested functionality and cleaned flame sensor
7. Tested functionality and cleaned pressure switches and ports
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Tested functionality and visually inspected surface igniter
12. Checked blower amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.

Upon testing the media room unit, it was found that the blower motor was not working. Further testing revealed that the motor was receiving signal from the con

Shelby S.

Shelby S. Job Checkin

Upon arrival, I found that the outdoor unit had lost high voltage due to a tripped breaker. I began diagnosing by checking for issues that would cause the breaker to trip. I found that the compressor has become short to ground. I verified warranty on the equipment. It is coverage until 2028. The route to repair is either compressor replacement or system replacement. With a compressor replacement, it is necessary to put virgin (unused) refrigerant back into system and replace the refrigerant filter dryer. An estimate was generated for labor, refrigerant, and refrigerant filter dryer. Also, I observed that the drain has become clogged since last service. Both the upstairs and downstairs drains are tied together. Jacob and I have both offered compressor savers for both systems and customer has declined them on multiple occasions.

Upon arrival, I found that the outdoor unit had lost high voltage due to a tripped breaker. I began diagnosing by checking for issues that would cause the breaker to trip. I found that the compressor has become short to ground. I verified warranty on the equipment. It is coverage until 2028. The route to repair is either compressor replacement or system replacement. With a compressor replacement, it is necessary to put virgin (unused) refrigerant back into system and replace the refrigerant filter dryer. An estimate was generated for labor, refrigerant, and refrigerant filter dryer. Also, I observed that the drain has become clogged since last service. Both the upstairs and downstairs drains are tied together. 

Jacob and I have both offered compressor savers for both systems and customer has declined them on multiple occasions. Upon arrival, I found that the outdoor unit had lost high voltage due to a tripped breaker. I began diagnosing by checking for issues that would cause the breaker to trip. I found that the compressor has become short to ground. I verified warranty on the equipment. It is coverage until 2028. The route to repair is either compressor replacement or system replacement. With a compressor replacement, it is necessary to put virgin (unused) refrigerant back into system and replace the refrigerant filter dryer. An estimate was generated for labor, refrigerant, and refrigerant filter dryer. Also, I observed that the drain has become clogged since last service. Both the upstairs and downstairs drains are tied together. 

Jacob and I have both offered compressor savers for both systems and customer has declined them on multiple occasions.

Brayden W.

Brayden W. Job Checkin

performed heating maintenance. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Inspected flame sensor and igniter 6. Tested pressure switches and various safeties for functionality 7. Tested normal operation of burners 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked inducer motor amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Replaced downstairs filter but did not have another filter to replace the upstairs. Homeowner has ordered and will replace. Unit in good working order upon departure

performed heating maintenance. 
1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Inspected flame sensor and igniter
6. Tested pressure switches and various safeties for functionality
7. Tested normal operation of burners 
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Inspected blower motor/ blower wheel.
12. Checked inducer motor amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.
14. Inspected drain lines and treated to prevent blockages 
15. Replaced downstairs filter but did not have another filter to replace the upstairs. Homeowner has ordered and will replace.

Unit in good working order upon departure performed heating maintenance. 
1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Inspected flame sensor and igniter
6. Tested pressure switches and various safeties for functionality
7. Tested normal operation of burners 
8. Inspected / replaced return filter.
9. Inspected return plenum for debris/ dirty.
10. Inspected evaporator coil.
11. Inspected blower motor/ blower wheel.
12. Checked inducer motor amp draw.
13. Measured temperature differential from supply to return. 20 degrees measured.
14. Inspected drain lines and treated to prevent blockages 
15. Replaced downstairs filter but did not have another filter to replace the upstairs. Homeowner has ordered and will replace.

Unit in good working order upon departure

Shelby S.

Shelby S. Job Checkin

I performed a 2 system heating maintenance on 2018 heat pump systems. I checked amps, capacitors, filters, electrical, cleanliness, heat kits, and safeties. I found that both systems are in need of cleaning, the blower motor on the upstairs unit is missing the keeper screw causing it emit a scrapping noise and damaging the motor itself, both u/v sticks are burnt out, and both outdoor units need hard start kits. I produced options to address these issues. Home owner was not home at the time of service, and I emailed options over for review. I was informed about areas of the downstairs being uncomfortable due to over cooling. I inspected the zoning system. I noticed that the dampers were set to allow air to all areas to the house to relieve pressure inside of the system. I adjusted the dampers to stop allowing air to “bleed” into other areas of the home. I confirmed the system has a bypass, but doing this may cause an issue.

I performed a 2 system heating maintenance on 2018 heat pump systems. I checked amps, capacitors, filters, electrical, cleanliness, heat kits, and safeties. I found that both systems are in need of cleaning, the blower motor on the upstairs unit is missing the keeper screw causing it emit a scrapping noise and damaging the motor itself, both u/v sticks are burnt out, and both outdoor units need hard start kits. I produced options to address these issues. Home owner was not home at the time of service, and I emailed options over for review. 
I was informed about areas of the downstairs being uncomfortable due to over cooling. I inspected the zoning system. I noticed that the dampers were set to allow air to all areas to the house to relieve pressure inside of the system. I adjusted the dampers to stop allowing air to “bleed” into other areas of the home. I confirmed the system has a bypass, but doing this may cause an issue. I performed a 2 system heating maintenance on 2018 heat pump systems. I checked amps, capacitors, filters, electrical, cleanliness, heat kits, and safeties. I found that both systems are in need of cleaning, the blower motor on the upstairs unit is missing the keeper screw causing it emit a scrapping noise and damaging the motor itself, both u/v sticks are burnt out, and both outdoor units need hard start kits. I produced options to address these issues. Home owner was not home at the time of service, and I emailed options over for review. 
I was informed about areas of the downstairs being uncomfortable due to over cooling. I inspected the zoning system. I noticed that the dampers were set to allow air to all areas to the house to relieve pressure inside of the system. I adjusted the dampers to stop allowing air to “bleed” into other areas of the home. I confirmed the system has a bypass, but doing this may cause an issue.

Shelby S.

Shelby S. Job Checkin

Demand call for upstairs system not cooling properly and having iced over. Customer did thaw out the system and the ice was cleared by the time we got here. Found the filter to be dirty, customer stated it’s only been in there for a month. Turned the system on and checked pressures and found the system to be low. Performed a leak search on indoor coil and couldn’t find anything. The outside coil has leak coming from the high pressure switch stem. Customer was outside with us and was able to see the leak himself with the soap bubbles we used. Our install crew is scheduled to come out tomorrow at 9am to do the repair.

Demand call for upstairs system not cooling properly and having iced over. Customer did thaw out the system and the ice was cleared by the time we got here. 
Found the filter to be dirty, customer stated it’s only been in there for a month. Turned the system on and checked pressures and found the system to be low. 
Performed a leak search on indoor coil and couldn’t find anything. The outside coil has leak coming from the high pressure switch stem. Customer was outside with us and was able to see the leak himself with the soap bubbles we used. 
Our install crew is scheduled to come out tomorrow at 9am to do the repair.

Brayden W.

Brayden W. Job Checkin

1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked safety sensors and pressure switch 7. Checked condenser fan motor amp draw. 8. Inspected return filter 9. Inspected return plenum for debris 10. Measured temperature differential from supply to return. 20 degrees measured. 11. Inspected drain lines and treated to prevent blockages and treated 12. Tested and cleaned flame sensor. Service switch at furnace stopped working after cycling power. Unwired switch and all was working as intended. All is well unit regards to normal unit operation. Unit in good working order upon departure.

1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Checked safety sensors and pressure switch
7. Checked condenser fan motor amp draw.
8. Inspected return filter
9. Inspected return plenum for debris
10. Measured temperature differential from supply to return. 20 degrees measured.
11. Inspected drain lines and treated to prevent blockages and treated
12. Tested and cleaned flame sensor.
Service switch at furnace stopped working after cycling power. Unwired switch and all was working as intended.
All is well unit regards to normal unit operation. Unit in good working order upon departure. 1. Visually inspected condenser coil for debris/ dirty.
2. Inspected condenser fan motor.
3. Inspected condenser fan blades.
4. Inspected/ cleaned wiring connections.
5. Tested compressor/ condenser fan motor capacitor.
6. Checked safety sensors and pressure switch
7. Checked condenser fan motor amp draw.
8. Inspected return filter
9. Inspected return plenum for debris
10. Measured temperature differential from supply to return. 20 degrees measured.
11. Inspected drain lines and treated to prevent blockages and treated
12. Tested and cleaned flame sensor.
Service switch at furnace stopped working after cycling power. Unwired switch and all was working as intended.
All is well unit regards to normal unit operation. Unit in good working order upon departure.

Jacob P.

Jacob P. Job Checkin

***Trail for 30 days before collecting payment*** Returned to home to install wireless temperature sensor to the upstairs thermostat. I connected the sensor and gave it 100% temperature control for the zone. Paul asked if we could put the sensor in his son’s bedroom. This room has a half dome window without shade. Once we placed the sensor in this space we allowed it to adjust on its own and it reached the existing set point of 73º. The thermostat displays the temperature read by the wireless sensor and we discussed the importance of changing the batteries to ensure the upstairs space stays comfortable. The wireless sensor reached the 73º set point and shut off the unit. This is an immediate sign that the system is functioning and cooling properly and that the residual heat affecting the wall mounted thermostat should no longer be an issue. We will still give Paul 30 day trail before charging the card on file.

***Trail for 30 days before collecting payment***

Returned to home to install wireless temperature sensor to the upstairs thermostat. I connected the sensor and gave it 100% temperature control for the zone. Paul asked if we could put the sensor in his son’s bedroom. This room has a half dome window without shade. Once we placed the sensor in this space we allowed it to adjust on its own and it reached the existing set point of 73º. The thermostat displays the temperature read by the wireless sensor and we discussed the importance of changing the batteries to ensure the upstairs space stays comfortable.

The wireless sensor reached the 73º set point and shut off the unit. This is an immediate sign that the system is functioning and cooling properly and that the residual heat affecting the wall mounted thermostat should no longer be an issue. We will still give Paul 30 day trail before charging the card on file. ***Trail for 30 days before collecting payment***

Returned to home to install wireless temperature sensor to the upstairs thermostat. I connected the sensor and gave it 100% temperature control for the zone. Paul asked if we could put the sensor in his son’s bedroom. This room has a half dome window without shade. Once we placed the sensor in this space we allowed it to adjust on its own and it reached the existing set point of 73º. The thermostat displays the temperature read by the wireless sensor and we discussed the importance of changing the batteries to ensure the upstairs space stays comfortable.

The wireless sensor reached the 73º set point and shut off the unit. This is an immediate sign that the system is functioning and cooling properly and that the residual heat affecting the wall mounted thermostat should no longer be an issue. We will still give Paul 30 day trail before charging the card on file.