He is very polite and patient. Explains all the options I have and provided great service. Thanks!
Our A/C broke when the weather started to get hot. We called Adon Complete, and Charles came. He was experienced and professional. He and his crew replaced our 20-year old unit, and our system is up and running just in time for summer. I would recommend Adon Complete for all my friends and neighbors.
I arrived at our clients home for a second opinion regarding their HVAC equipment. I met with Shonna and she educated me regarding the situation. She showed me her thermostat and attic access and I proceeded to inspect the equipment. I did ask for permission to also diagnose the system to potentially provide a fix. I found the system to be completely empty on refrigerant and other minor issues related to ductwork. I found the system to have double filter (one in the ceiling and another in the attic). I did not create an estimate for repairs due to the age and obvious signs that the system has a significant refrigerant leak. I did created 2 estimates options and will be sending them to both via email. I also addressed the email Mr. Brown sent to us 1. Outdoor Condenser Unit (brand, model, SEER2 rating, and tonnage recommended) - American Standard 15.2 SEER 5 Ton Conventional split system 2. Indoor Coil / Evaporator (brand/model, compatibility with condenser)- 5 ton Matching American
Upon arrival, I found that majority of the grills are covered in a growth. Home owner was on site during this visit. I removed 2 grills and found that the supply boots are not sealed. Also, I found that the home has high humidity. I told the customer, we need these units to run for longer periods of time and to leave the fan on auto. I measured all of the grills (review pictures for sizes), and I discussed sealing the supply boots during grill replacement. The estimate that will be provided will include sealing the supply boots. I noticed that the downstairs thermostat may be getting teased by the living room supply vent, also. All of the vents are 3 way vents.
I returned to our clients home to install two collars with dampers for the attic space. The objective is to condition the attic and help reduce the humidity in the attic and home.
Arrived to the upstairs unit not cooling properly. I first went into the attic and verified the indoor unit was on. I then proceeded outside and found that the capacitor had failed. Our technician had recommended replacement during the maintenance in June. Because the capacitor had failed it had caused the compressor to cross into a lockout due to high temperature. I took the time to cool it down and ensure it would turn on again. I called the homeowner and recommended a Hardstart kit with the replacement capacitor to help keep the compressor within normal manufacture specifications. He elected to move forward with the repair. I let the unit run and measured the temperature in the attic. It is cooling properly on departure, with a 20° drop. The outdoor fan motor had high start amps and has clear visible signs of overheating as well. I did not have a replacement motor to potentially recommend this repair but will send an estimate for its replacement.
I performed a single system maintenance on a 2009 R22 gas system. I checked amps, capacitor, filter, drains, electrical, cleanliness, and safeties. I found the ground wire for the blower motor not hooked up and a couple of loose connections on the control board. I secured the ground wire and tightened the loose connections. I noticed the unit has a 15 degree temperature drop. I informed the customer that I believe this unit has 2 years left at best. The duct work has a responsible amount of dust contributory the dirty blower motor. I advised that these should be cleaned to remove stress from the system. The customer would like to make it through summer before considering replacement. I noticed that the contactor wasn’t in the best condition, the unit had an unnecessary fan motor capacitor, and that the unit was starting with higher amps. I priced duct cleaning for the customer, installed a 2 pole contactor, and offered a hard start kit. The system is performing to the best of its abili
Upon arrival we noticed the 3/5 outdoor units were extremely caked with cotton wood debris. We brought this to managements attention and they went ahead with the chemical cleaning on those three units. We then preformed cooling maintenance on all of the units. We tested start and run amps on all outdoor electrical components and found that 1(trane) unit was starting on the high side. All other electrical components on each of the systems tested within manufacture specifications. We tested electrical components on each inside unit all tested within manufacture specifications. We treated drain lines with total c to help prevent clogs. We did notice one of the emergency drain pans had some rust build up in the bottom. Which could potentially lead to a leak in the ceiling if the unit were to get clogged and go into that drain pan. Temperature splits on all the units were within 18- 20 degrees. Units were cooling upon departure. 521 ELECTRONIC HARD START 189-227 UF 170-277V 1 HP AND
I arrived at our client home for concerns that the mini split in the garage was leaking water and damaging the wood paneled ceiling. I was able to locate the primary drain line from the mini split to the master bedroom unit and confirmed it was plumbed into that primary drain line. I then opened the two side panels to the cassette unit and looked into the cavity space where the cassette is located. I found the drain line but it had no evidence or fleas or condensation coming from it. The drywall above the “wet spot” of the wood was dry with no evidence of moisture. I showed these pictures to Scott and we discussed possible options to install a iflow drain cleaner as well as a service valve and T to actively remove water from the drain line. He elected to install the blowout valve and T today and I showed him before and after pictures of the work preformed. I also went into the upstairs attic and we discussed adding a return and supply vent to the front area downstairs unit to help con
Objective: To install an exhaust fan in the ceiling of the media room closet to help ventilate and cool the area containing high-performance AV equipment. The goal is to pull cooler air through the closet and discharge hot air into the attic space, preventing overheating and maintaining optimal equipment performance. ⸻ Work Description: 1. Exhaust Fan Installation • Install a high-performance exhaust fan in the ceiling of the media room closet. • The fan will pull cooler ambient air through the closet and discharge the hot air into the attic space above. • Installation will ensure minimal noise and vibration while maximizing airflow. 2. Thermostat and Controls • Install a wall-mounted thermostat in the closet to control the exhaust fan based on temperature. • Thermostat will not adjust room temperature but will act as a temperature-sensitive switch for the exhaust fan. • System will include a relay and a low-voltage transformer to operate the fan based on thermostat readings
Upon arrival the office staff said the ac was not cooling but the fan was running. We proceeded to the riser room to gain roof access. Upon inspection of the unit we found that the compressor and coils were frozen over. We are unable to determine the issue until unit can thaw out and we can properly diagnose the issues. Spoke to the owner and confirmed we would need to come back in the morning. Unit was not cooling but fan was running upon departure.
Arrived on site customer complained of theater room getting too warm and daughters bedroom getting too cold. Adjusted airflow as best we could to push more air to theatre and slightly less to daughter’s room. Closed off damper to upstairs main area with thermostat. May need an additional supply and larger return to accommodate customers preferences. 1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser uni
1. Visually inspected condenser coil for debris/ dirty. 2. Inspected condenser fan motor. 3. Inspected condenser fan blades. 4. Inspected/ cleaned wiring connections. 5. Tested compressor/ condenser fan motor capacitor. 6. Checked compressor amp draw. 7. Checked condenser fan motor amp draw. 8. Inspected / replaced return filter. 9. Inspected return plenum for debris/ dirty. 10. Inspected evaporator coil. 11. Inspected blower motor/ blower wheel. 12. Checked blower amp draw. 13. Measured temperature differential from supply to return. 20 degrees measured. 14. Inspected drain lines and treated to prevent blockages 15. Washed condenser unit to promote heat exchange Upstairs unit bad compressor capacitor. Informed customer of possibility of unit failure due to capacitor failure. Customer wanted to monitor the capacitor and proceed if it gets worse or fails. Notified customer of temperature sensor with dead batteries. Customer replaced batteries error went away.
I arrived at our clients home for the unit not cooling properly. I was first led into the home and into the attic. Everything appeared to be working properly and the filter was in good condition. I then went outside and found the outdoor compressor not running. I further diagnosed a failed capacitor to the compressor motor. I did further test the contactor and ensured the system had standing refrigerant. I showed my findings to Mr Adam’s and we discussed the capacitor replacement as well as adding a compressor saver tot he outdoor unit today. Mr Adam’s elected to replace the capacitor only today. Once replaced I further tested and the system to ensure proper operation. I did measure a good 20° drop in the attic. The compressor however is exceeding is manufacturing amp limit. It started up at 166 out of 146 amps today. I did a lite rinse of the outdoor coils to also help the system breathe and operate better. The Freon pressures are a little low. Mr Adam’s is aware this R22 refriger
I arrived at our clients home to preform a single system cooling maintenance. I went through and answered Mr Obryan’s questions regarding the maintenance and what we provided in the cooling and heat in services. We first proceeded into the attic and did a visual inspection on the AirHandler. I then went outside and began to test all the electrical components on the outdoor heat pump. I first rinsed the outdoor coils with water. After that I found several components with visible signs of failure and also were reading close to failure according to manufacturer specifications. I went back into the attic and checked the temperature drop at the air handler. Mr OBryan had several windows and doors open when checking refrigerant pressures and temperatures but I was still getting a 17° drop. I went back into the attic and tested the electrical components for the AirHandler. I found another compromised contactor and a capacitor that failed my test today. I showed all my findings to our client
I found the upstairs unit low on R410a. I called and received approval to install leak seal and 5 pounds of R410a. System is now cooling and dropping temperature upstairs.