725 Kintner Parkway
Sunbury, OH 43074
614-827-1259

Local Reviews
for gahanna, oh

Rated 5.0 out of 5 stars based on 3 customer reviews

Excellent service, would recommend to anyone

Fixed the problems. Additionally, cleaned the coils in my air conditioner, showed me what the problem was and how it was to be repaired. He did NOT try to sell to me contracts for maintenance or any other unnecessary at the time service. I will use them again.

  • Overall Experience
  • Quality
  • Price
  • Convenience

good service

Explained what he did to tweak my system and why. Let me know if there were any additional needs, he would come back to readjust to my satisfaction.

  • Overall Experience
  • Quality
  • Price
  • Convenience

Clearing the Air

Representative was courteous, thorough and efficient in his review, cleaning and prepping of our heating and air conditioning system for the summer months ahead.

  • Overall Experience
  • Quality
  • Price
  • Convenience

Job Locations
for gahanna, oh

Jason D.

Jason D. Job Checkin

Install new 200,000 BTU Reznor gas unit heater Equipment: REZ-UDXC-200, PWR.VENT 82-83% UNIT HTR 200MB Serial# B2A3062004628 *Honeywell thermostat Installation: *Reconnect to existing gas line and high voltage electric *Start up and commission the new equipment *Westin Air to use customer provided scissor lift or fork lift *Westin Air will remove and recycle old unit Warranty: Reznor commercial parts warranty 1 Year Westin Air labor warranty


Install new 200,000 BTU Reznor gas unit heater
Equipment: REZ-UDXC-200, PWR.VENT 82-83% UNIT HTR 200MB
Serial# B2A3062004628
*Honeywell thermostat

Installation:
*Reconnect to existing gas line and high voltage electric
*Start up and commission the new equipment
*Westin Air to use customer provided scissor lift or fork lift
*Westin Air will remove and recycle old unit

Warranty:
Reznor commercial parts warranty
1 Year Westin Air labor warranty



Install new 200,000 BTU Reznor gas unit heater
Equipment: REZ-UDXC-200, PWR.VENT 82-83% UNIT HTR 200MB
Serial# B2A3062004628
*Honeywell thermostat

Installation:
*Reconnect to existing gas line and high voltage electric
*Start up and commission the new equipment
*Westin Air to use customer provided scissor lift or fork lift
*Westin Air will remove and recycle old unit

Warranty:
Reznor commercial parts warranty
1 Year Westin Air labor warranty

Jason D.

Jason D. Job Checkin

Install new Bryant HVAC heat pump system Equipment: Air Handler-FJ5ANXB30L00 Puron AdvanceTM Legacy Series Fan Coil Serial# 4925F31556 Heat Pump-GH5SAN53000A 14.3 SEER2 Single-Stage Heat Pump with Puron Advance Refrigerant, R-454B, 2.5 Ton, 208/230V Serial# 1725X24627 *15KW Aux heat *Honeywell PRO heat pump thermostat Installation: *Reconnect to existing high voltage electric circuits *Transition to existing supply and return ductwork *Start up and commission the new system Warranty: 10 Year Bryant manufacturers parts warranty (Annual maintenance must be performed) 2 Year Westin Air labor warranty (Annual maintenance must be performed)


Nate G.

Nate G. Job Checkin

20 year old Goodman heat pump system 15 kilowatt auxiliary heat pack only operating at 5kw. Two of the three heat strips have failed Incorrect filter size has been in place for an unknown amount of time Indoor air coil is plugged with dirt as a result Heat pump is performing below specification System cannot keep up with heating demands Recommend full system replacement

20 year old Goodman heat pump system 
15 kilowatt auxiliary heat pack only operating at 5kw.  Two of the three heat strips have failed
Incorrect filter size has been in place for an unknown amount of time
Indoor air coil is plugged with dirt as a result
Heat pump is performing below specification
System cannot keep up with heating demands

Recommend full system replacement 20 year old Goodman heat pump system 
15 kilowatt auxiliary heat pack only operating at 5kw.  Two of the three heat strips have failed
Incorrect filter size has been in place for an unknown amount of time
Indoor air coil is plugged with dirt as a result
Heat pump is performing below specification
System cannot keep up with heating demands

Recommend full system replacement

Nate G.

Nate G. Job Checkin

Replace gas valve


Brandon P.

Brandon P. Job Checkin

Preventative maintenence inspection on Trane standard efficiency furnace running in good condition. 16x25x1 air filter is new today. Clean flame sensor and check ignitor. Visual inspection of burners. Test blower capacitor. Run test unit in heating mode from thermostat. Temperature rise is within specs. Blower and inducer motors tested good. 4" galvanized B-vent in good condition and no sign of leaks. 0PPM CO detected during testing. System is operating properly, efficiently and ready for Winter.


Brandon P.

Brandon P. Job Checkin

Preventative maintenence inspection on Tempstar gas furnace running in good condition. 20x25x4 air filter replaced today. Clean flame sensor and check ignitor ohms. Flush condensation trap and drain lines. Run test unit in heating mode from thermostat. Temperature rise is within specs. Blower and inducer motors tested good. Pvc flue vents in good condition and no sign of leaks. 0PPM CO detected during testing. System is operating properly, efficiently and ready for Winter.


Nate G.

Nate G. Job Checkin

Service recall: maintenance performed less than 30 days ago Found no 120V power coming into the furnace Disconnect switch failed from having the wires stabbed in rather than wrapped around the screws Bypassed failed switch Furnace would still not power up despite having 120V to it now Verified 24V at transformer secondary Pulled 3A fuse from the control board, it was blown Checked for short circuits with Ohm meter, nothing found Replaced fuse and powered on furnace It went through its startup routine and when it energized the gas valve, the fuse blew again Replaced gas valve and fuse Set gas pressure to 3.5"wc Furnace operating normally at this time


Brandon P.

Brandon P. Job Checkin

Preventative maintenence inspection on Armstrong Air furnace running in good condition. 16x25x1 air filter is new today. Clean flame sensor and check ignitor. Visual inspection of burners. Run test furnace in heating mode from thermostat. Temperature rise is within specs. Blower and inducer motors tested good. 4" galvanized B-vent in good condition and no sign of leaks. 0PPM CO detected during testing. System is operating properly, efficiently and ready for Winter.


Nate G.

Nate G. Job Checkin

Performed heating maintenance on a 2019 Trane two stage 80% efficient natural gas furnace 20x24x1 filter is new today Blower wheel is clean Pulled flame sensor and cleaned Modified thermostat wiring to allow thermostat to control furnace heat staging. Also set dip switches on control board for no time delay on a 2nd stage call for heat Run tested furnace High fire gas pressure set to 3.5"wc Temperature rise 44⁰ Low fire gas pressure set to 1.7"wc Temperature rise 46⁰ Temperature rise specification range is 35-65⁰ Furnace is in great shape and operating perfectly within manufacturer's specifications at this time


Nate G.

Nate G. Job Checkin

Expansion valve (TXV) on indoor coil is not regulating refrigerant flow properly. Indoor coil is starved for refrigerant Pumped refrigerant back to outdoor unit Flowed nitrogen through the system to keep moisture and air out while system was open Replaced TXV. Pressure tested to 400psi Released nitrogen from the system Connected vacuum pump Pulled down to 300 microns Performed ten minute decay test Vacuum rose to 740 microns after 10 minutes Pulled vacuum down to 260 microns for an additional 10 minutes Opened valves to release refrigerant back to the indoor coil Started up system All numbers are nominal for the current indoor and outdoor conditions

Expansion valve (TXV) on indoor coil is not regulating refrigerant flow properly.
Indoor coil is starved for refrigerant

Pumped refrigerant back to outdoor unit
Flowed nitrogen through the system to keep moisture and air out while system was open
Replaced TXV.  
Pressure tested to 400psi
Released nitrogen from the system
Connected vacuum pump
Pulled down to 300 microns
Performed ten minute decay test
Vacuum rose to 740 microns after 10 minutes
Pulled vacuum down to 260 microns for an additional 10 minutes 
Opened valves to release refrigerant back to the indoor coil
Started up system
All numbers are nominal for the current indoor and outdoor conditions Expansion valve (TXV) on indoor coil is not regulating refrigerant flow properly.
Indoor coil is starved for refrigerant

Pumped refrigerant back to outdoor unit
Flowed nitrogen through the system to keep moisture and air out while system was open
Replaced TXV.  
Pressure tested to 400psi
Released nitrogen from the system
Connected vacuum pump
Pulled down to 300 microns
Performed ten minute decay test
Vacuum rose to 740 microns after 10 minutes
Pulled vacuum down to 260 microns for an additional 10 minutes 
Opened valves to release refrigerant back to the indoor coil
Started up system
All numbers are nominal for the current indoor and outdoor conditions

Graham M.

Graham M. Job Checkin

Performed gold cooling maintenance Filter new Blower clean Drain clear Only getting 12.5⁰ delta T across evaporator coil Pulled coil door off, no signs of freezing Top half of the coil is dry Connected refrigerant probes to outdoor unit Charge specification is 10⁰ +/-3⁰ for liquid line subcooling Getting 9⁰ subcool, charge level is correct Suction pressure is a little low Superheat is very high @32⁰... should be more like 10⁰ Expansion valve needs replaced under factory parts warranty Checked all wiring Capacitor tested at rated specification Everything else with the system is in good shape

Performed gold cooling maintenance 
Filter new
Blower clean
Drain clear
Only getting 12.5⁰ delta T across evaporator coil
Pulled coil door off, no signs of freezing
Top half of the coil is dry
Connected refrigerant probes to outdoor unit
Charge specification is 10⁰ +/-3⁰ for liquid line subcooling
Getting 9⁰ subcool, charge level is correct 
Suction pressure is a little low
Superheat is very high @32⁰... should be more like 10⁰
Expansion valve needs replaced under factory parts warranty
Checked all wiring
Capacitor tested at rated specification 
Everything else with the system is in good shape

Nate G.

Nate G. Job Checkin

Service recall Unit requires 30A breaker Installed square D 30A two pole breaker Unit operating normally.


Graham M.

Graham M. Job Checkin

Unit is operational at this time. Cooling but cannot check head pressure valve core broken. Attempted to replace but core is snapped off inside valve. Unit cannot be properly inspected. Could tell coil was clogged on condenser because of airflow problems up top, fan has suction in center and blowing out on outer rim. Unit cannot operate properly during peak heat due to venting issues. Unit should be replaced for best results

Unit is operational at this time. Cooling but cannot check head pressure valve core broken. Attempted to replace but core is snapped off inside valve. Unit cannot be properly inspected. Could tell coil was clogged on condenser because of airflow problems up top, fan has suction in center and blowing out on outer rim. Unit cannot operate properly during peak heat due to venting issues. Unit should be replaced for best results Unit is operational at this time. Cooling but cannot check head pressure valve core broken. Attempted to replace but core is snapped off inside valve. Unit cannot be properly inspected. Could tell coil was clogged on condenser because of airflow problems up top, fan has suction in center and blowing out on outer rim. Unit cannot operate properly during peak heat due to venting issues. Unit should be replaced for best results

Graham M.

Graham M. Job Checkin

Upon arrival found 1 tripped breaker for system. Unit getting 120v not 240v. Reset power and check amp draw. Nothing pulling high amps currently, swapped out all the wire nuts I used when motor was replaced for butt connectors to avoid potential amperage increase. Unit is cooling with 11° subcool. Pulling 9.8 amps total


Graham M.

Graham M. Job Checkin

Remove and replace condenser motor due to motor reversed and stuck in clockwise direction when motor should be counterclockwise. Setup new motor CCW on 1/6hp 240v 5mfd capacitor black does not get used red and white are used and capacitor wires are now yellow and blue. Wash coil