2930 61st Street
Menomonie, WI 54751
715-283-4422

Our Top Cities


Local Reviews
for shoreview, mn


Job Locations
for shoreview, mn

Charles P.

Charles P. Job Checkin

Replaced malfunctioning gas pressure regulator on exterior gas line serving home's fireplaces. Removed corroded T-fitting and installed new regulator with appropriate connections and valves to ensure proper gas pressure to system. Completed all necessary testing to verify safe operation.

Replaced malfunctioning gas pressure regulator on exterior gas line serving home's fireplaces. Removed corroded T-fitting and installed new regulator with appropriate connections and valves to ensure proper gas pressure to system. Completed all necessary testing to verify safe operation. Replaced malfunctioning gas pressure regulator on exterior gas line serving home's fireplaces. Removed corroded T-fitting and installed new regulator with appropriate connections and valves to ensure proper gas pressure to system. Completed all necessary testing to verify safe operation.

Moe R.

Moe R. Job Checkin

Responded to service call for gas fireplaces not operating. Upon inspection, found the gas regulator at the exterior meter requires replacement. Informed customer this work falls under gas utility jurisdiction and advised them to contact their provider for the necessary repairs.

Responded to service call for gas fireplaces not operating. Upon inspection, found the gas regulator at the exterior meter requires replacement. Informed customer this work falls under gas utility jurisdiction and advised them to contact their provider for the necessary repairs. Responded to service call for gas fireplaces not operating. Upon inspection, found the gas regulator at the exterior meter requires replacement. Informed customer this work falls under gas utility jurisdiction and advised them to contact their provider for the necessary repairs.

Scott N

Scott N Job Checkin

Responded to new customer service call to replace laundry sink faucet. Customer had purchased new faucet but installation was prevented by deteriorated pipes and shut-off valves. Completed replacement of both faucet and valves with customer-supplied components.

Responded to new customer service call to replace laundry sink faucet. Customer had purchased new faucet but installation was prevented by deteriorated pipes and shut-off valves. Completed replacement of both faucet and valves with customer-supplied components. Responded to new customer service call to replace laundry sink faucet. Customer had purchased new faucet but installation was prevented by deteriorated pipes and shut-off valves. Completed replacement of both faucet and valves with customer-supplied components.

Charles P.

Charles P. Job Checkin

Responded to service call for non-functional garbage disposal in kitchen sink. Diagnostic inspection revealed seized disposal unit. Removed defective unit and installed new replacement garbage disposal. Tested operation to confirm proper functionality.

Responded to service call for non-functional garbage disposal in kitchen sink. Diagnostic inspection revealed seized disposal unit. Removed defective unit and installed new replacement garbage disposal. Tested operation to confirm proper functionality. Responded to service call for non-functional garbage disposal in kitchen sink. Diagnostic inspection revealed seized disposal unit. Removed defective unit and installed new replacement garbage disposal. Tested operation to confirm proper functionality.

Charles P.

Charles P. Job Checkin

Diagnosed and repaired leaking American Standard two-handle bathroom faucet by replacing faulty cartridge that wasn't seating properly. Discovered and replaced 12 deteriorated angle stop valves throughout the residence (bathroom and kitchen fixtures) as they were 25 years old and not completely shutting off water flow.

Diagnosed and repaired leaking American Standard two-handle bathroom faucet by replacing faulty cartridge that wasn't seating properly. Discovered and replaced 12 deteriorated angle stop valves throughout the residence (bathroom and kitchen fixtures) as they were 25 years old and not completely shutting off water flow. Diagnosed and repaired leaking American Standard two-handle bathroom faucet by replacing faulty cartridge that wasn't seating properly. Discovered and replaced 12 deteriorated angle stop valves throughout the residence (bathroom and kitchen fixtures) as they were 25 years old and not completely shutting off water flow.

Tony C.

Tony C. Job Checkin

Responded to customer report of a leaking exposed pipe in the basement. Diagnosed and confirmed kitchen drain line with a rusted T-junction. Replaced the damaged section with new PVC P-trap assembly, including elbow joints and unions, ensuring proper connections to existing metal drain component. Work successfully resolved the leak issue.

Responded to customer report of a leaking exposed pipe in the basement. Diagnosed and confirmed kitchen drain line with a rusted T-junction. Replaced the damaged section with new PVC P-trap assembly, including elbow joints and unions, ensuring proper connections to existing metal drain component. Work successfully resolved the leak issue.

Roger M.

Roger M. Job Checkin

Performed annual maintenance tune-up on 8-year-old Amana HVAC system. Inspected ductwork and internal components. Identified stripped gas valve adjustment, which was replaced to restore proper functionality. System operational upon completion.

Performed annual maintenance tune-up on 8-year-old Amana HVAC system. Inspected ductwork and internal components. Identified stripped gas valve adjustment, which was replaced to restore proper functionality. System operational upon completion. Performed annual maintenance tune-up on 8-year-old Amana HVAC system. Inspected ductwork and internal components. Identified stripped gas valve adjustment, which was replaced to restore proper functionality. System operational upon completion.

Jon W

Jon W Job Checkin

Responded to a no heat complaint in a vacant property with furnace short cycling due to overheating. Diagnosed multiple issues: inducer draft motor failing and causing improper exhaust ventilation, incorrectly sized filter boot restricting proper airflow, and excessive gas pressure in low fire (over 2" wc, above the 1.3"-1.7" manufacturer range). Adjusted gas pressure down to 1.38" wc, removed filter, and restored proper heat operation with extended run cycles.

Responded to a no heat complaint in a vacant property with furnace short cycling due to overheating. Diagnosed multiple issues: inducer draft motor failing and causing improper exhaust ventilation, incorrectly sized filter boot restricting proper airflow, and excessive gas pressure in low fire (over 2" wc, above the 1.3"-1.7" manufacturer range). Adjusted gas pressure down to 1.38" wc, removed filter, and restored proper heat operation with extended run cycles. Responded to a no heat complaint in a vacant property with furnace short cycling due to overheating. Diagnosed multiple issues: inducer draft motor failing and causing improper exhaust ventilation, incorrectly sized filter boot restricting proper airflow, and excessive gas pressure in low fire (over 2" wc, above the 1.3"-1.7" manufacturer range). Adjusted gas pressure down to 1.38" wc, removed filter, and restored proper heat operation with extended run cycles.

Roger M.

Roger M. Job Checkin

Performed comprehensive furnace tune-up on 10-year-old system. Cleaned dirty flame sensor and replaced filter. Conducted gas pressure testing with dual port manometer, verifying proper operation at 15.7 WC supply and -10.1 WC draft. Inspected blower assembly and internal components for proper condition and functionality.

Performed comprehensive furnace tune-up on 10-year-old system. Cleaned dirty flame sensor and replaced filter. Conducted gas pressure testing with dual port manometer, verifying proper operation at 15.7 WC supply and -10.1 WC draft. Inspected blower assembly and internal components for proper condition and functionality. Performed comprehensive furnace tune-up on 10-year-old system. Cleaned dirty flame sensor and replaced filter. Conducted gas pressure testing with dual port manometer, verifying proper operation at 15.7 WC supply and -10.1 WC draft. Inspected blower assembly and internal components for proper condition and functionality.

Jon W

Jon W Job Checkin

Responded to no heat complaint where unit was blowing cold air. Diagnostic testing revealed a failed control board. Successfully replaced control board, restoring proper heating function to the aging system.

Responded to no heat complaint where unit was blowing cold air. Diagnostic testing revealed a failed control board. Successfully replaced control board, restoring proper heating function to the aging system. Responded to no heat complaint where unit was blowing cold air. Diagnostic testing revealed a failed control board. Successfully replaced control board, restoring proper heating function to the aging system.

Jon W

Jon W Job Checkin

Performed furnace inspection and tune-up service. Combustion analysis showed system operating at 87.5% efficiency with acceptable CO levels (5 ppm). Identified multiple critical issues including failing ignition components, oil leakage from blower motor, burn marks on control board, and contaminated secondary heat exchanger. Recommended either component replacement or complete furnace replacement due to the extent of deterioration.

Performed furnace inspection and tune-up service. Combustion analysis showed system operating at 87.5% efficiency with acceptable CO levels (5 ppm). Identified multiple critical issues including failing ignition components, oil leakage from blower motor, burn marks on control board, and contaminated secondary heat exchanger. Recommended either component replacement or complete furnace replacement due to the extent of deterioration. Performed furnace inspection and tune-up service. Combustion analysis showed system operating at 87.5% efficiency with acceptable CO levels (5 ppm). Identified multiple critical issues including failing ignition components, oil leakage from blower motor, burn marks on control board, and contaminated secondary heat exchanger. Recommended either component replacement or complete furnace replacement due to the extent of deterioration.

Tim M.

Tim M. Job Checkin

Repaired a leaking ABS drain pipe in the laundry area that was causing water to drip into the mechanical room. Discovered a crack between the 4-way hub and 2" wye that couldn't be salvaged. Capped the 2" hub and installed a new wye lower in the stack to properly redirect the bath group drainage and venting.

Repaired a leaking ABS drain pipe in the laundry area that was causing water to drip into the mechanical room. Discovered a crack between the 4-way hub and 2" wye that couldn't be salvaged. Capped the 2" hub and installed a new wye lower in the stack to properly redirect the bath group drainage and venting.

Jarrod S.

Jarrod S. Job Checkin

Performed comprehensive inspection of reported gas leak at client's furnace supply line. After thorough assessment using detection equipment, no active gas leaks were identified in the system. Also investigated sewer line for reported root intrusion; visual inspection confirmed no current blockage from tree roots. Documentation photos taken of existing plumbing assembly showing copper supply lines, valves, and connection points in structural space.

Performed comprehensive inspection of reported gas leak at client's furnace supply line. After thorough assessment using detection equipment, no active gas leaks were identified in the system. Also investigated sewer line for reported root intrusion; visual inspection confirmed no current blockage from tree roots. Documentation photos taken of existing plumbing assembly showing copper supply lines, valves, and connection points in structural space. Performed comprehensive inspection of reported gas leak at client's furnace supply line. After thorough assessment using detection equipment, no active gas leaks were identified in the system. Also investigated sewer line for reported root intrusion; visual inspection confirmed no current blockage from tree roots. Documentation photos taken of existing plumbing assembly showing copper supply lines, valves, and connection points in structural space.

Xavier C.

Xavier C. Job Checkin

Performed routine maintenance on 11-year-old Ruud furnace. Cleaned flame sensor, verified proper ignitor operation, and confirmed good amp draws on inducer and blower motors. System is operating safely with appropriate gas pressures, clean filter, clear condensation drains, and sound electrical components.

Performed routine maintenance on 11-year-old Ruud furnace. Cleaned flame sensor, verified proper ignitor operation, and confirmed good amp draws on inducer and blower motors. System is operating safely with appropriate gas pressures, clean filter, clear condensation drains, and sound electrical components. Performed routine maintenance on 11-year-old Ruud furnace. Cleaned flame sensor, verified proper ignitor operation, and confirmed good amp draws on inducer and blower motors. System is operating safely with appropriate gas pressures, clean filter, clear condensation drains, and sound electrical components.

Xavier C.

Xavier C. Job Checkin

Diagnosed and repaired 10-year-old HVAC system that was failing to cool properly. Investigation revealed a faulty capacitor preventing the outdoor condensing unit from operating correctly. Replaced the defective capacitor and verified proper system operation with post-repair diagnostics showing appropriate refrigerant pressures (100.3 PSI suction, 151.5 PSI liquid).

Diagnosed and repaired 10-year-old HVAC system that was failing to cool properly. Investigation revealed a faulty capacitor preventing the outdoor condensing unit from operating correctly. Replaced the defective capacitor and verified proper system operation with post-repair diagnostics showing appropriate refrigerant pressures (100.3 PSI suction, 151.5 PSI liquid). Diagnosed and repaired 10-year-old HVAC system that was failing to cool properly. Investigation revealed a faulty capacitor preventing the outdoor condensing unit from operating correctly. Replaced the defective capacitor and verified proper system operation with post-repair diagnostics showing appropriate refrigerant pressures (100.3 PSI suction, 151.5 PSI liquid).