2930 61st Street
Menomonie, WI 54751
715-283-4422

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Local Reviews
for baldwin, wi

Rated 4.5 out of 5 stars based on 2 customer reviews

The new faucet looks great

I had Hurlburts out to replace a kitchen faucet, the guy did a great job and really took care to protect our house. Well trained technician and you can tell the company has high standards.


Response from Hurlburt Heating & Plumbing:

We’re so glad you had a good experience.

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Mike is the BEST!

Mike has been coming to my house for over 10 years, he's just a good man that I trust in my home. I wish there were more people like this these days!


Response from Hurlburt Heating & Plumbing:

Thank you for sharing your kind words with us. It means the world to us and to our entire team!

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Job Locations
for baldwin, wi

Gary L.

Gary L. Job Checkin

Performed scheduled maintenance on 25-year-old Bryant 80% furnace. Cleaned dirty blower wheel and documented system age. Informed homeowner about system condition; husband performs repairs as needed. Replaced air filter during service.

Performed scheduled maintenance on 25-year-old Bryant 80% furnace. Cleaned dirty blower wheel and documented system age. Informed homeowner about system condition; husband performs repairs as needed. Replaced air filter during service. Performed scheduled maintenance on 25-year-old Bryant 80% furnace. Cleaned dirty blower wheel and documented system age. Informed homeowner about system condition; husband performs repairs as needed. Replaced air filter during service.

Jeremy N.

Jeremy N. Job Checkin

Diagnosed toilet not refilling after flush; discovered frozen and leaking 1/2" CPVC supply line. Replaced damaged section with new 1/2" PEX pipe, installed new shut-off valve and supply line to toilet, and connected to existing CPVC via 1/2" Sharkbite coupling to restore proper function.

Diagnosed toilet not refilling after flush; discovered frozen and leaking 1/2" CPVC supply line. Replaced damaged section with new 1/2" PEX pipe, installed new shut-off valve and supply line to toilet, and connected to existing CPVC via 1/2" Sharkbite coupling to restore proper function. Diagnosed toilet not refilling after flush; discovered frozen and leaking 1/2" CPVC supply line. Replaced damaged section with new 1/2" PEX pipe, installed new shut-off valve and supply line to toilet, and connected to existing CPVC via 1/2" Sharkbite coupling to restore proper function.

Ben W.

Ben W. Job Checkin

Diagnosed RTU failure to operate heating function. Verified voltage at thermostat heat terminal but observed no inducer motor operation despite proper voltage supply to motor. Determined inducer motor requires replacement. Noted and documented UV damage to external wiring harness, which was reported to maintenance personnel. Customer requested pricing for both inducer motor replacement and complete unit replacement options.

Diagnosed RTU failure to operate heating function. Verified voltage at thermostat heat terminal but observed no inducer motor operation despite proper voltage supply to motor. Determined inducer motor requires replacement. Noted and documented UV damage to external wiring harness, which was reported to maintenance personnel. Customer requested pricing for both inducer motor replacement and complete unit replacement options.

Kegan M.

Kegan M. Job Checkin

Responded to service call for no hot water in upstairs bathroom. Diagnosed issue with water lines located in outside wall causing restricted flow to upstairs fixtures. Recommended repiping solution to resolve the problem, but customer opted to defer this repair due to cost considerations. Inspected cast iron drainage system and existing plumbing configuration in basement area.

Responded to service call for no hot water in upstairs bathroom. Diagnosed issue with water lines located in outside wall causing restricted flow to upstairs fixtures. Recommended repiping solution to resolve the problem, but customer opted to defer this repair due to cost considerations. Inspected cast iron drainage system and existing plumbing configuration in basement area. Responded to service call for no hot water in upstairs bathroom. Diagnosed issue with water lines located in outside wall causing restricted flow to upstairs fixtures. Recommended repiping solution to resolve the problem, but customer opted to defer this repair due to cost considerations. Inspected cast iron drainage system and existing plumbing configuration in basement area.

Noah S

Noah S Job Checkin

Performed complementary flush of tankless water heater using haymaker solution as scheduled. Inspected existing copper plumbing system and connections in basement utility area. Completed full system flush to remove mineral buildup and ensure optimal operation of the on-demand water heater.

Performed complementary flush of tankless water heater using haymaker solution as scheduled. Inspected existing copper plumbing system and connections in basement utility area. Completed full system flush to remove mineral buildup and ensure optimal operation of the on-demand water heater. Performed complementary flush of tankless water heater using haymaker solution as scheduled. Inspected existing copper plumbing system and connections in basement utility area. Completed full system flush to remove mineral buildup and ensure optimal operation of the on-demand water heater.

Bryson E.

Bryson E. Job Checkin

Responded to warranty service call for recently installed water heater producing a constant squealing sound. Diagnostic inspection revealed a minor gas valve leak seeping into the combustion chamber, causing the noise. Initiated parts order for replacement gas valve to resolve the issue.

Responded to warranty service call for recently installed water heater producing a constant squealing sound. Diagnostic inspection revealed a minor gas valve leak seeping into the combustion chamber, causing the noise. Initiated parts order for replacement gas valve to resolve the issue. Responded to warranty service call for recently installed water heater producing a constant squealing sound. Diagnostic inspection revealed a minor gas valve leak seeping into the combustion chamber, causing the noise. Initiated parts order for replacement gas valve to resolve the issue.

Craig M.

Craig M. Job Checkin

Responded to no heat call for aging furnace. Diagnosed issue with furnace cycling frequently due to severely clogged filter and continuous humidifier operation causing overheating. Replaced filter and tested system operation, noting reduced fan performance, dirty wheel and coil. Discussed previously provided replacement quote with homeowner and addressed concerns about winter installation timing.

Responded to no heat call for aging furnace. Diagnosed issue with furnace cycling frequently due to severely clogged filter and continuous humidifier operation causing overheating. Replaced filter and tested system operation, noting reduced fan performance, dirty wheel and coil. Discussed previously provided replacement quote with homeowner and addressed concerns about winter installation timing.

Ben W.

Ben W. Job Checkin

Diagnosed no-heat issue on 8-year-old Daikin furnace by identifying clogged pressure switch port on collector box. Performed remediation including port cleaning, drain flush, flame sensor cleaning, heat exchanger inspection, and burner check. Replaced burners as preventative measure due to debris accumulation in gas channel, ensuring proper ignition and system operation.

Diagnosed no-heat issue on 8-year-old Daikin furnace by identifying clogged pressure switch port on collector box. Performed remediation including port cleaning, drain flush, flame sensor cleaning, heat exchanger inspection, and burner check. Replaced burners as preventative measure due to debris accumulation in gas channel, ensuring proper ignition and system operation. Diagnosed no-heat issue on 8-year-old Daikin furnace by identifying clogged pressure switch port on collector box. Performed remediation including port cleaning, drain flush, flame sensor cleaning, heat exchanger inspection, and burner check. Replaced burners as preventative measure due to debris accumulation in gas channel, ensuring proper ignition and system operation.

Doug T.

Doug T. Job Checkin

Responded to emergency service call for toilet leak between wall and shut-off valve. Diagnosed water supply issue at connection point. Replaced defective shut-off valve and water supply line. Recommended toilet replacement due to condition of existing fixture.

Responded to emergency service call for toilet leak between wall and shut-off valve. Diagnosed water supply issue at connection point. Replaced defective shut-off valve and water supply line. Recommended toilet replacement due to condition of existing fixture. Responded to emergency service call for toilet leak between wall and shut-off valve. Diagnosed water supply issue at connection point. Replaced defective shut-off valve and water supply line. Recommended toilet replacement due to condition of existing fixture.

Beca R.

Beca R. Job Checkin

Responded to warranty call for newly installed furnace reporting high-pitched squealing noise during startup. Conducted thorough inspection of unit including gas valve and airflow components. Unit did not reproduce the reported noise during service visit, preventing definitive diagnosis. Customer advised potential causes include gas valve operation or airflow issues that will require follow-up if noise persists.

Responded to warranty call for newly installed furnace reporting high-pitched squealing noise during startup. Conducted thorough inspection of unit including gas valve and airflow components. Unit did not reproduce the reported noise during service visit, preventing definitive diagnosis. Customer advised potential causes include gas valve operation or airflow issues that will require follow-up if noise persists. Responded to warranty call for newly installed furnace reporting high-pitched squealing noise during startup. Conducted thorough inspection of unit including gas valve and airflow components. Unit did not reproduce the reported noise during service visit, preventing definitive diagnosis. Customer advised potential causes include gas valve operation or airflow issues that will require follow-up if noise persists.

Ben W.

Ben W. Job Checkin

Performed diagnostic inspection on zone valve system and identified need for power head replacement. Upon arrival, discovered incorrect replacement part was provided. Documented existing valve configuration with photos showing copper piping assembly and internal components of the current zone valve head. Service to be completed on return visit with proper replacement parts sourced from alternate location.

Performed diagnostic inspection on zone valve system and identified need for power head replacement. Upon arrival, discovered incorrect replacement part was provided. Documented existing valve configuration with photos showing copper piping assembly and internal components of the current zone valve head. Service to be completed on return visit with proper replacement parts sourced from alternate location. Performed diagnostic inspection on zone valve system and identified need for power head replacement. Upon arrival, discovered incorrect replacement part was provided. Documented existing valve configuration with photos showing copper piping assembly and internal components of the current zone valve head. Service to be completed on return visit with proper replacement parts sourced from alternate location.

Trent L.

Trent L. Job Checkin

Responded to service call for a furnace repeatedly shutting down overnight requiring morning resets. Diagnosed issue as overheating caused by severely clogged air filter which customer had just replaced. Performed comprehensive system check including cleaning flame sensor, verifying proper condensate drainage, and confirming correct gas pressure. System now operating normally with appropriate 55° temperature rise. Advised customer on importance of regular filter maintenance.

Responded to service call for a furnace repeatedly shutting down overnight requiring morning resets. Diagnosed issue as overheating caused by severely clogged air filter which customer had just replaced. Performed comprehensive system check including cleaning flame sensor, verifying proper condensate drainage, and confirming correct gas pressure. System now operating normally with appropriate 55° temperature rise. Advised customer on importance of regular filter maintenance. Responded to service call for a furnace repeatedly shutting down overnight requiring morning resets. Diagnosed issue as overheating caused by severely clogged air filter which customer had just replaced. Performed comprehensive system check including cleaning flame sensor, verifying proper condensate drainage, and confirming correct gas pressure. System now operating normally with appropriate 55° temperature rise. Advised customer on importance of regular filter maintenance.

David B.

David B. Job Checkin

Diagnosed and replaced faulty control board on ceiling-mounted unit heater in workshop. Performed complete system testing after installation to verify proper operation of all heating functions. Unit now functioning correctly with restored temperature control capabilities.

Diagnosed and replaced faulty control board on ceiling-mounted unit heater in workshop. Performed complete system testing after installation to verify proper operation of all heating functions. Unit now functioning correctly with restored temperature control capabilities. Diagnosed and replaced faulty control board on ceiling-mounted unit heater in workshop. Performed complete system testing after installation to verify proper operation of all heating functions. Unit now functioning correctly with restored temperature control capabilities.

David B.

David B. Job Checkin

Replaced defective 3" PVC exhaust pipe system due to multiple leaks discovered during inspection. Corrected improper intake and exhaust terminations that were not to code. Installed new complete exhaust piping with proper outdoor terminations to ensure safe and compliant operation of the HVAC system.

Replaced defective 3" PVC exhaust pipe system due to multiple leaks discovered during inspection. Corrected improper intake and exhaust terminations that were not to code. Installed new complete exhaust piping with proper outdoor terminations to ensure safe and compliant operation of the HVAC system. Replaced defective 3" PVC exhaust pipe system due to multiple leaks discovered during inspection. Corrected improper intake and exhaust terminations that were not to code. Installed new complete exhaust piping with proper outdoor terminations to ensure safe and compliant operation of the HVAC system.

Ben W.

Ben W. Job Checkin

Performed annual furnace maintenance on 4-year-old FRP system. Conducted operational testing, gas pressure verification, and temperature rise check. Identified and remediated two issues: applied necessary silicone to unsealed exhaust PVC connection at furnace top and diagnosed leaking 3" PVC joint. Provided customer with options for humidifier installation and discussed potential solutions for bathroom ventilation and additional return air installations.

Performed annual furnace maintenance on 4-year-old FRP system. Conducted operational testing, gas pressure verification, and temperature rise check. Identified and remediated two issues: applied necessary silicone to unsealed exhaust PVC connection at furnace top and diagnosed leaking 3" PVC joint. Provided customer with options for humidifier installation and discussed potential solutions for bathroom ventilation and additional return air installations. Performed annual furnace maintenance on 4-year-old FRP system. Conducted operational testing, gas pressure verification, and temperature rise check. Identified and remediated two issues: applied necessary silicone to unsealed exhaust PVC connection at furnace top and diagnosed leaking 3" PVC joint. Provided customer with options for humidifier installation and discussed potential solutions for bathroom ventilation and additional return air installations.