2930 61st Street
Menomonie, WI 54751
715-283-4422

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Roger M.

Roger M. Job Checkin

Successfully replaced gas valve on LP furnace. Unable to adjust gas pressure due to empty LP tank. Customer scheduled for LP delivery, will return after fill to complete pressure calibration.

Successfully replaced gas valve on LP furnace. Unable to adjust gas pressure due to empty LP tank. Customer scheduled for LP delivery, will return after fill to complete pressure calibration. Successfully replaced gas valve on LP furnace. Unable to adjust gas pressure due to empty LP tank. Customer scheduled for LP delivery, will return after fill to complete pressure calibration.

Koshoua V.

Koshoua V. Job Checkin

Responded to no-heat call for Goodman furnace. Diagnostic testing revealed hot surface igniter functioning correctly and gas valve receiving power, but zero gas pressure at inlet/outlet. Resistance testing confirmed failed gas valve, which was replaced to restore proper heating operation.

Responded to no-heat call for Goodman furnace. Diagnostic testing revealed hot surface igniter functioning correctly and gas valve receiving power, but zero gas pressure at inlet/outlet. Resistance testing confirmed failed gas valve, which was replaced to restore proper heating operation. Responded to no-heat call for Goodman furnace. Diagnostic testing revealed hot surface igniter functioning correctly and gas valve receiving power, but zero gas pressure at inlet/outlet. Resistance testing confirmed failed gas valve, which was replaced to restore proper heating operation.

Ali T

Ali T Job Checkin

Diagnosed primary heat exchanger failure in 30+ year old forced air furnace. Furnace was experiencing intermittent blower operation. Upon inspection of internal components and electrical connections, identified cracked heat exchanger which poses carbon monoxide safety risk. Tagged equipment as unsafe for operation and scheduled for replacement estimate.

Diagnosed primary heat exchanger failure in 30+ year old forced air furnace. Furnace was experiencing intermittent blower operation. Upon inspection of internal components and electrical connections, identified cracked heat exchanger which poses carbon monoxide safety risk. Tagged equipment as unsafe for operation and scheduled for replacement estimate. Diagnosed primary heat exchanger failure in 30+ year old forced air furnace. Furnace was experiencing intermittent blower operation. Upon inspection of internal components and electrical connections, identified cracked heat exchanger which poses carbon monoxide safety risk. Tagged equipment as unsafe for operation and scheduled for replacement estimate.

Koshoua V.

Koshoua V. Job Checkin

Performed comprehensive furnace tune-up on a unit that had not been operated for 2 years. Inspection revealed properly functioning system with normal operation. Services included heat exchanger inspection, combustion analysis testing, gas pressure verification (both high and low stage), flame sensor and burner inspection, and blower motor evaluation. Secured condensate tube connection after clearing water buildup. Air filter in moderate condition, pressure switch cleaned. Thermostat confirmed operational with adequate heating performance. No immediate concerns identified.

Performed comprehensive furnace tune-up on a unit that had not been operated for 2 years. Inspection revealed properly functioning system with normal operation. Services included heat exchanger inspection, combustion analysis testing, gas pressure verification (both high and low stage), flame sensor and burner inspection, and blower motor evaluation. Secured condensate tube connection after clearing water buildup. Air filter in moderate condition, pressure switch cleaned. Thermostat confirmed operational with adequate heating performance. No immediate concerns identified. Performed comprehensive furnace tune-up on a unit that had not been operated for 2 years. Inspection revealed properly functioning system with normal operation. Services included heat exchanger inspection, combustion analysis testing, gas pressure verification (both high and low stage), flame sensor and burner inspection, and blower motor evaluation. Secured condensate tube connection after clearing water buildup. Air filter in moderate condition, pressure switch cleaned. Thermostat confirmed operational with adequate heating performance. No immediate concerns identified.

Kegan M.

Kegan M. Job Checkin

Successfully installed customer-supplied LP gas water heater (Richmond model) in unfinished basement area. Properly connected black insulated pipes to the top of the unit and positioned the heater adjacent to customer's blue WaterMate tank. Noted presence of mineral deposits on exterior of tank, likely from previous unit.

Successfully installed customer-supplied LP gas water heater (Richmond model) in unfinished basement area. Properly connected black insulated pipes to the top of the unit and positioned the heater adjacent to customer's blue WaterMate tank. Noted presence of mineral deposits on exterior of tank, likely from previous unit. Successfully installed customer-supplied LP gas water heater (Richmond model) in unfinished basement area. Properly connected black insulated pipes to the top of the unit and positioned the heater adjacent to customer's blue WaterMate tank. Noted presence of mineral deposits on exterior of tank, likely from previous unit.

Koshoua V.

Koshoua V. Job Checkin

Performed comprehensive furnace tuneup on 2-year-old LP unit. Cleared condensation drain line and trap of accumulated spiderwebbing and debris. Verified proper operation of inducer motor, pressure switch, control board connections, and thermostat. Combustion analysis showed CO at 13 ppm, within acceptable range. System operating normally with no immediate concerns. Filter in moderate condition.

Performed comprehensive furnace tuneup on 2-year-old LP unit. Cleared condensation drain line and trap of accumulated spiderwebbing and debris. Verified proper operation of inducer motor, pressure switch, control board connections, and thermostat. Combustion analysis showed CO at 13 ppm, within acceptable range. System operating normally with no immediate concerns. Filter in moderate condition. Performed comprehensive furnace tuneup on 2-year-old LP unit. Cleared condensation drain line and trap of accumulated spiderwebbing and debris. Verified proper operation of inducer motor, pressure switch, control board connections, and thermostat. Combustion analysis showed CO at 13 ppm, within acceptable range. System operating normally with no immediate concerns. Filter in moderate condition.

Koshoua V.

Koshoua V. Job Checkin

Performed comprehensive furnace tune-up including clearing condensate drain line and trap of accumulated debris. Inspected heat exchanger which revealed multiple rust eyelids, advised homeowner to install carbon monoxide detector. Verified proper operation of all major components (inducer motor, capacitor, pressure switch, control board connections, thermostat), cleaned flame sensor, and replaced filter.

Performed comprehensive furnace tune-up including clearing condensate drain line and trap of accumulated debris. Inspected heat exchanger which revealed multiple rust eyelids, advised homeowner to install carbon monoxide detector. Verified proper operation of all major components (inducer motor, capacitor, pressure switch, control board connections, thermostat), cleaned flame sensor, and replaced filter. Performed comprehensive furnace tune-up including clearing condensate drain line and trap of accumulated debris. Inspected heat exchanger which revealed multiple rust eyelids, advised homeowner to install carbon monoxide detector. Verified proper operation of all major components (inducer motor, capacitor, pressure switch, control board connections, thermostat), cleaned flame sensor, and replaced filter.

Ali T

Ali T Job Checkin

Responded to no-heat call for a 13-year-old Lennox furnace (Model G61MPV-36B-071-12, SN: 5910J04984). Diagnostic testing revealed failed inducer motor capacitor. Replaced capacitor and confirmed proper system operation, restoring heat functionality with thermostat now properly calling for heat at 70°F setpoint.

Responded to no-heat call for a 13-year-old Lennox furnace (Model G61MPV-36B-071-12, SN: 5910J04984). Diagnostic testing revealed failed inducer motor capacitor. Replaced capacitor and confirmed proper system operation, restoring heat functionality with thermostat now properly calling for heat at 70°F setpoint. Responded to no-heat call for a 13-year-old Lennox furnace (Model G61MPV-36B-071-12, SN: 5910J04984). Diagnostic testing revealed failed inducer motor capacitor. Replaced capacitor and confirmed proper system operation, restoring heat functionality with thermostat now properly calling for heat at 70°F setpoint.

Koshoua V.

Koshoua V. Job Checkin

Performed semi-annual FRP Furnace Tune Up on 12-42 year-old unit. Tested and confirmed gas train pressure at 9.32 inWC, cleaned condensate drain line and trap to remove debris and spiderwebbing, and verified CO levels at 15 ppm. Inspected and confirmed proper operation of inducer motor, capacitor, pressure switch, control board connections, and thermostat. Replaced moderately soiled return air filter with new one. Furnace is operating within normal parameters with no immediate concerns identified.

Performed semi-annual FRP Furnace Tune Up on 12-42 year-old unit. Tested and confirmed gas train pressure at 9.32 inWC, cleaned condensate drain line and trap to remove debris and spiderwebbing, and verified CO levels at 15 ppm. Inspected and confirmed proper operation of inducer motor, capacitor, pressure switch, control board connections, and thermostat. Replaced moderately soiled return air filter with new one. Furnace is operating within normal parameters with no immediate concerns identified. Performed semi-annual FRP Furnace Tune Up on 12-42 year-old unit. Tested and confirmed gas train pressure at 9.32 inWC, cleaned condensate drain line and trap to remove debris and spiderwebbing, and verified CO levels at 15 ppm. Inspected and confirmed proper operation of inducer motor, capacitor, pressure switch, control board connections, and thermostat. Replaced moderately soiled return air filter with new one. Furnace is operating within normal parameters with no immediate concerns identified.

Roger M.

Roger M. Job Checkin

Diagnosed garage ceiling-mounted heating unit that was cycling on briefly then shutting down. Determined gas valve was malfunctioning - valve would initially open but then fail during operation. Replaced faulty gas valve to restore proper heating function.

Diagnosed garage ceiling-mounted heating unit that was cycling on briefly then shutting down. Determined gas valve was malfunctioning - valve would initially open but then fail during operation. Replaced faulty gas valve to restore proper heating function. Diagnosed garage ceiling-mounted heating unit that was cycling on briefly then shutting down. Determined gas valve was malfunctioning - valve would initially open but then fail during operation. Replaced faulty gas valve to restore proper heating function.

Xavier C.

Xavier C. Job Checkin

Diagnosed garage heater with no-heat condition and found stuck gas valve and high gas pressure setting. Restored temporary operation by manually freeing valve and calibrating gas pressure to correct specifications. Recommended gas valve replacement to prevent recurrence of the issue.

Diagnosed garage heater with no-heat condition and found stuck gas valve and high gas pressure setting. Restored temporary operation by manually freeing valve and calibrating gas pressure to correct specifications. Recommended gas valve replacement to prevent recurrence of the issue. Diagnosed garage heater with no-heat condition and found stuck gas valve and high gas pressure setting. Restored temporary operation by manually freeing valve and calibrating gas pressure to correct specifications. Recommended gas valve replacement to prevent recurrence of the issue.

Trevor P.

Trevor P. Job Checkin

Performed maintenance inspection on an inactive barn furnace that hasn't operated for several years. Discovered improper horizontal venting installation contrary to manufacturer specifications requiring vertical venting, and noted complete absence of ductwork and LP gas supply. Successfully tested ignition sequence to verify ignitor glow and gas valve operation. Recommended proper vertical venting installation per manufacturer requirements, addition of necessary ductwork, and suggested possible replacement with a hanging heater as potentially more suitable for the application.

Performed maintenance inspection on an inactive barn furnace that hasn't operated for several years. Discovered improper horizontal venting installation contrary to manufacturer specifications requiring vertical venting, and noted complete absence of ductwork and LP gas supply. Successfully tested ignition sequence to verify ignitor glow and gas valve operation. Recommended proper vertical venting installation per manufacturer requirements, addition of necessary ductwork, and suggested possible replacement with a hanging heater as potentially more suitable for the application. Performed maintenance inspection on an inactive barn furnace that hasn't operated for several years. Discovered improper horizontal venting installation contrary to manufacturer specifications requiring vertical venting, and noted complete absence of ductwork and LP gas supply. Successfully tested ignition sequence to verify ignitor glow and gas valve operation. Recommended proper vertical venting installation per manufacturer requirements, addition of necessary ductwork, and suggested possible replacement with a hanging heater as potentially more suitable for the application.

Dan S.

Dan S. Job Checkin

Diagnosed noise concerns in customer's HVAC systems. Found heat pump noise was normal operation during defrost cycle, but identified locked inducer motor on natural gas furnace requiring replacement. Also inspected barn woodstove with locked fan motor; noted parts may be difficult to source as manufacturer is no longer in business. Prepared estimates and parts orders for both repair issues.

Diagnosed noise concerns in customer's HVAC systems. Found heat pump noise was normal operation during defrost cycle, but identified locked inducer motor on natural gas furnace requiring replacement. Also inspected barn woodstove with locked fan motor; noted parts may be difficult to source as manufacturer is no longer in business. Prepared estimates and parts orders for both repair issues. Diagnosed noise concerns in customer's HVAC systems. Found heat pump noise was normal operation during defrost cycle, but identified locked inducer motor on natural gas furnace requiring replacement. Also inspected barn woodstove with locked fan motor; noted parts may be difficult to source as manufacturer is no longer in business. Prepared estimates and parts orders for both repair issues.

Dan S.

Dan S. Job Checkin

Responded to no-heat service call for a first-generation Heil furnace. Upon inspection, identified cracked secondary heat exchanger with water and combustion gas leakage. Visual inspection with camera confirmed failure to customer. Due to safety concerns and component failure, recommended complete system replacement. Scheduled follow-up consultation with service advisor for replacement options.

Responded to no-heat service call for a first-generation Heil furnace. Upon inspection, identified cracked secondary heat exchanger with water and combustion gas leakage. Visual inspection with camera confirmed failure to customer. Due to safety concerns and component failure, recommended complete system replacement. Scheduled follow-up consultation with service advisor for replacement options. Responded to no-heat service call for a first-generation Heil furnace. Upon inspection, identified cracked secondary heat exchanger with water and combustion gas leakage. Visual inspection with camera confirmed failure to customer. Due to safety concerns and component failure, recommended complete system replacement. Scheduled follow-up consultation with service advisor for replacement options.

Bryson E.

Bryson E. Job Checkin

Successfully installed customer-supplied garbage disposal, ran refrigerator water line for ice maker, and replaced outdoor spigot (had to cut hose as it could not be detached). Secured all connections and verified proper operation.

Successfully installed customer-supplied garbage disposal, ran refrigerator water line for ice maker, and replaced outdoor spigot (had to cut hose as it could not be detached). Secured all connections and verified proper operation. Successfully installed customer-supplied garbage disposal, ran refrigerator water line for ice maker, and replaced outdoor spigot (had to cut hose as it could not be detached). Secured all connections and verified proper operation.