2930 61st Street
Menomonie, WI 54751
715-283-4422

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for elk mound, wi

Rated 5.0 out of 5 stars based on 1 customer reviews

Best Air Conditioner Guys Around!

I hate the heat so I'm not about to take a chance on anyone else. Just call Hurlburt, they know their stuff.


Response from Hurlburt Heating & Plumbing:

Thank you so much for taking the time to leave an excellent rating. We really appreciate your business.

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Job Locations
for elk mound, wi

Andrew M.

Andrew M. Job Checkin

Installed customer-supplied American Standard double flapper toilet, connecting new braided stainless steel supply line to existing brass shutoff valve. Also installed customer-provided kitchen sink and faucet as requested. All fixtures were properly secured and tested for leaks after installation.

Installed customer-supplied American Standard double flapper toilet, connecting new braided stainless steel supply line to existing brass shutoff valve. Also installed customer-provided kitchen sink and faucet as requested. All fixtures were properly secured and tested for leaks after installation.

Mike B.

Mike B. Job Checkin

Responded to no heat complaint on 5-year-old furnace with intermittent shutdown issues. Diagnostic testing revealed flame loss codes in system memory. Performed maintenance service including flame sensor cleaning and gas pressure verification (found slightly low at 9.8" inlet, 4.8" manifold). System operated continuously during 30-minute observation period after service. Recommended replacement of both house and tank regulators through propane company if issues persist.

Responded to no heat complaint on 5-year-old furnace with intermittent shutdown issues. Diagnostic testing revealed flame loss codes in system memory. Performed maintenance service including flame sensor cleaning and gas pressure verification (found slightly low at 9.8" inlet, 4.8" manifold). System operated continuously during 30-minute observation period after service. Recommended replacement of both house and tank regulators through propane company if issues persist. Responded to no heat complaint on 5-year-old furnace with intermittent shutdown issues. Diagnostic testing revealed flame loss codes in system memory. Performed maintenance service including flame sensor cleaning and gas pressure verification (found slightly low at 9.8" inlet, 4.8" manifold). System operated continuously during 30-minute observation period after service. Recommended replacement of both house and tank regulators through propane company if issues persist.

Dan S.

Dan S. Job Checkin

Responded to no heat call for Amana LP furnace. Diagnosed completely plugged furnace filter caused by ultrasonic humidifiers as source of issue. Reset limit switch after filter replacement, restoring normal operation. Performed visual inspection of heat exchanger and burners, confirmed system is in good working condition for its age. Advised customer about proper humidification options.

Responded to no heat call for Amana LP furnace. Diagnosed completely plugged furnace filter caused by ultrasonic humidifiers as source of issue. Reset limit switch after filter replacement, restoring normal operation. Performed visual inspection of heat exchanger and burners, confirmed system is in good working condition for its age. Advised customer about proper humidification options. Responded to no heat call for Amana LP furnace. Diagnosed completely plugged furnace filter caused by ultrasonic humidifiers as source of issue. Reset limit switch after filter replacement, restoring normal operation. Performed visual inspection of heat exchanger and burners, confirmed system is in good working condition for its age. Advised customer about proper humidification options.

Noah S

Noah S Job Checkin

Repaired water leak at tub valve body by identifying a pin hole leak in the brass fitting. Accessed plumbing infrastructure through wall cutout, installed crimp fittings to successfully resolve the leak issue and restore proper function to the shower/tub water connection.

Repaired water leak at tub valve body by identifying a pin hole leak in the brass fitting. Accessed plumbing infrastructure through wall cutout, installed crimp fittings to successfully resolve the leak issue and restore proper function to the shower/tub water connection. Repaired water leak at tub valve body by identifying a pin hole leak in the brass fitting. Accessed plumbing infrastructure through wall cutout, installed crimp fittings to successfully resolve the leak issue and restore proper function to the shower/tub water connection.

Beca R.

Beca R. Job Checkin

Inspected furnace in response to noise complaints and heating failure. Internal examination of ductwork revealed multiple collapsed sections with significant dust accumulation, restricting proper airflow. Advised customer that blower motor is beginning to fail due to restricted airflow conditions and recommended complete ductwork replacement prior to motor replacement to prevent damage to new components and ensure proper system function.

Inspected furnace in response to noise complaints and heating failure. Internal examination of ductwork revealed multiple collapsed sections with significant dust accumulation, restricting proper airflow. Advised customer that blower motor is beginning to fail due to restricted airflow conditions and recommended complete ductwork replacement prior to motor replacement to prevent damage to new components and ensure proper system function. Inspected furnace in response to noise complaints and heating failure. Internal examination of ductwork revealed multiple collapsed sections with significant dust accumulation, restricting proper airflow. Advised customer that blower motor is beginning to fail due to restricted airflow conditions and recommended complete ductwork replacement prior to motor replacement to prevent damage to new components and ensure proper system function.

Jared R.

Jared R. Job Checkin

Diagnosed and resolved no-heat issue on 6-year-old gas furnace. Found open high limit switch due to severely clogged air filter, which was restricting proper airflow. Replaced air filter and performed comprehensive system check including ignitor, flame sensor, inducer, condensate drain, pressure switch, heat exchanger and burners. System restored to normal operation and now heating properly to thermostat setpoint.

Diagnosed and resolved no-heat issue on 6-year-old gas furnace. Found open high limit switch due to severely clogged air filter, which was restricting proper airflow. Replaced air filter and performed comprehensive system check including ignitor, flame sensor, inducer, condensate drain, pressure switch, heat exchanger and burners. System restored to normal operation and now heating properly to thermostat setpoint. Diagnosed and resolved no-heat issue on 6-year-old gas furnace. Found open high limit switch due to severely clogged air filter, which was restricting proper airflow. Replaced air filter and performed comprehensive system check including ignitor, flame sensor, inducer, condensate drain, pressure switch, heat exchanger and burners. System restored to normal operation and now heating properly to thermostat setpoint.

Gary L.

Gary L. Job Checkin

Responded to a customer complaint of gas odor originating from the garage heater. Upon inspection, identified a loose union fitting on the LP gas line serving the ceiling-mounted heating unit. Tightened the union fitting to secure the connection and eliminate the gas leak. Customer was informed of findings and resolution.

Responded to a customer complaint of gas odor originating from the garage heater. Upon inspection, identified a loose union fitting on the LP gas line serving the ceiling-mounted heating unit. Tightened the union fitting to secure the connection and eliminate the gas leak. Customer was informed of findings and resolution. Responded to a customer complaint of gas odor originating from the garage heater. Upon inspection, identified a loose union fitting on the LP gas line serving the ceiling-mounted heating unit. Tightened the union fitting to secure the connection and eliminate the gas leak. Customer was informed of findings and resolution.

Koshoua V.

Koshoua V. Job Checkin

Performed furnace tune-up on 5-year-old FRP unit that was running continuously without maintaining temperature. Diagnosed error codes E250 and E311 indicating restricted airflow. Determined high MERV 10 filter was causing restriction; replaced with lower MERV filter which reduced supply temperature from 160° to 115°. Replaced high limit switch, verified proper gas pressure and CO readings. System now operating normally with improved airflow.

Performed furnace tune-up on 5-year-old FRP unit that was running continuously without maintaining temperature. Diagnosed error codes E250 and E311 indicating restricted airflow. Determined high MERV 10 filter was causing restriction; replaced with lower MERV filter which reduced supply temperature from 160° to 115°. Replaced high limit switch, verified proper gas pressure and CO readings. System now operating normally with improved airflow. Performed furnace tune-up on 5-year-old FRP unit that was running continuously without maintaining temperature. Diagnosed error codes E250 and E311 indicating restricted airflow. Determined high MERV 10 filter was causing restriction; replaced with lower MERV filter which reduced supply temperature from 160° to 115°. Replaced high limit switch, verified proper gas pressure and CO readings. System now operating normally with improved airflow.

Beca R.

Beca R. Job Checkin

Responded to service call for intermittent furnace operation. Diagnosed issues with flame sensor and limit switches. Inspected 20-year-old unit that was cycling off prematurely. Cleaned flame sensor to remove white residue buildup and tested limit switch system. Verified proper operation after maintenance and confirmed system is currently functioning correctly.

Responded to service call for intermittent furnace operation. Diagnosed issues with flame sensor and limit switches. Inspected 20-year-old unit that was cycling off prematurely. Cleaned flame sensor to remove white residue buildup and tested limit switch system. Verified proper operation after maintenance and confirmed system is currently functioning correctly. Responded to service call for intermittent furnace operation. Diagnosed issues with flame sensor and limit switches. Inspected 20-year-old unit that was cycling off prematurely. Cleaned flame sensor to remove white residue buildup and tested limit switch system. Verified proper operation after maintenance and confirmed system is currently functioning correctly.

David B.

David B. Job Checkin

Responded to customer complaint of newly installed furnace not heating properly and producing excess heat in crawl space. Diagnostic inspection revealed three issues: clogged filter restricting airflow, improper furnace staging configuration, and frozen condensate pump drain line routed outside. Service completed by installing new filter, adjusting blower speeds for proper air distribution, and reconfiguring staging dip switches for optimal performance.

Responded to customer complaint of newly installed furnace not heating properly and producing excess heat in crawl space. Diagnostic inspection revealed three issues: clogged filter restricting airflow, improper furnace staging configuration, and frozen condensate pump drain line routed outside. Service completed by installing new filter, adjusting blower speeds for proper air distribution, and reconfiguring staging dip switches for optimal performance. Responded to customer complaint of newly installed furnace not heating properly and producing excess heat in crawl space. Diagnostic inspection revealed three issues: clogged filter restricting airflow, improper furnace staging configuration, and frozen condensate pump drain line routed outside. Service completed by installing new filter, adjusting blower speeds for proper air distribution, and reconfiguring staging dip switches for optimal performance.

Mike A.

Mike A. Job Checkin

Responded to no heat call for 25-year-old LP furnace with pressure switch error (three flash code). Diagnosed issue with pressure switch tubing, trimmed tubing and reinserted properly into inducer housing. System started successfully and maintained operation through multiple test cycles. Performed visual inspection of heat exchanger and cleaned flame sensor to ensure proper ignition. Unit functioning normally upon completion.

Responded to no heat call for 25-year-old LP furnace with pressure switch error (three flash code). Diagnosed issue with pressure switch tubing, trimmed tubing and reinserted properly into inducer housing. System started successfully and maintained operation through multiple test cycles. Performed visual inspection of heat exchanger and cleaned flame sensor to ensure proper ignition. Unit functioning normally upon completion. Responded to no heat call for 25-year-old LP furnace with pressure switch error (three flash code). Diagnosed issue with pressure switch tubing, trimmed tubing and reinserted properly into inducer housing. System started successfully and maintained operation through multiple test cycles. Performed visual inspection of heat exchanger and cleaned flame sensor to ensure proper ignition. Unit functioning normally upon completion.

Ethan S.

Ethan S. Job Checkin

Responded to no-heat call for a 10+ year old furnace that was shutting down after 30-60 seconds with flame sensing error. Diagnosed issue with dirty igniter despite acceptable ohm readings. Customer provided replacement igniter which was installed, restoring proper system operation. Unit identified as model M1MB 070A BW with serial MTB010305775.

Responded to no-heat call for a 10+ year old furnace that was shutting down after 30-60 seconds with flame sensing error. Diagnosed issue with dirty igniter despite acceptable ohm readings. Customer provided replacement igniter which was installed, restoring proper system operation. Unit identified as model M1MB 070A BW with serial MTB010305775. Responded to no-heat call for a 10+ year old furnace that was shutting down after 30-60 seconds with flame sensing error. Diagnosed issue with dirty igniter despite acceptable ohm readings. Customer provided replacement igniter which was installed, restoring proper system operation. Unit identified as model M1MB 070A BW with serial MTB010305775.

Kegan M.

Kegan M. Job Checkin

Inspected 40-gallon water heater with active leak requiring replacement. Identified additional plumbing issues including rattling pipes during water shutoff and deterioration of main sewer pipe connection showing significant rust buildup and leakage at union joint. Provided comprehensive assessment and replacement options for water heater system.

Inspected 40-gallon water heater with active leak requiring replacement. Identified additional plumbing issues including rattling pipes during water shutoff and deterioration of main sewer pipe connection showing significant rust buildup and leakage at union joint. Provided comprehensive assessment and replacement options for water heater system. Inspected 40-gallon water heater with active leak requiring replacement. Identified additional plumbing issues including rattling pipes during water shutoff and deterioration of main sewer pipe connection showing significant rust buildup and leakage at union joint. Provided comprehensive assessment and replacement options for water heater system.

Doug T.

Doug T. Job Checkin

Responded to no hot water complaint for Bradford White tanked water heater. Diagnosed intermittent pilot light failure caused by dirty flame sensor and broken glow rod (customer attempted self-repair). Cleaned flame sensor and replaced damaged component to restore proper ignition and hot water service.

Responded to no hot water complaint for Bradford White tanked water heater. Diagnosed intermittent pilot light failure caused by dirty flame sensor and broken glow rod (customer attempted self-repair). Cleaned flame sensor and replaced damaged component to restore proper ignition and hot water service. Responded to no hot water complaint for Bradford White tanked water heater. Diagnosed intermittent pilot light failure caused by dirty flame sensor and broken glow rod (customer attempted self-repair). Cleaned flame sensor and replaced damaged component to restore proper ignition and hot water service.

Ben W.

Ben W. Job Checkin

Responded to a no heat call where previous service had identified debris in pressure switch. Upon inspection, found additional debris buildup inside pressure switch port and exhaust ports. Cleared obstructions and verified furnace operation. Diagnosed weak flame signal indicated by flashing yellow light on control board. Determined igniter/flame sensor replacement needed, which will be ordered and installed on follow-up visit.

Responded to a no heat call where previous service had identified debris in pressure switch. Upon inspection, found additional debris buildup inside pressure switch port and exhaust ports. Cleared obstructions and verified furnace operation. Diagnosed weak flame signal indicated by flashing yellow light on control board. Determined igniter/flame sensor replacement needed, which will be ordered and installed on follow-up visit. Responded to a no heat call where previous service had identified debris in pressure switch. Upon inspection, found additional debris buildup inside pressure switch port and exhaust ports. Cleared obstructions and verified furnace operation. Diagnosed weak flame signal indicated by flashing yellow light on control board. Determined igniter/flame sensor replacement needed, which will be ordered and installed on follow-up visit.