2930 61st Street
Menomonie, WI 54751
715-283-4422

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for elk mound, wi

Rated 5.0 out of 5 stars based on 1 customer reviews

Best Air Conditioner Guys Around!

I hate the heat so I'm not about to take a chance on anyone else. Just call Hurlburt, they know their stuff.


Response from Hurlburt Heating & Plumbing:

Thank you so much for taking the time to leave an excellent rating. We really appreciate your business.

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Job Locations
for elk mound, wi

Trent L.

Trent L. Job Checkin

Responded to no heat call at property with Goodman furnace. Upon inspection, discovered extensive rodent infestation inside unit with nesting material throughout components. Internal examination revealed severe rusting and seized components due to previous basement flooding approximately six years ago. Multiple mice were observed within the heat exchanger area. After consultation with homeowner and demonstrating the extent of damage, recommended full system replacement as repairs would likely approach replacement cost.

Responded to no heat call at property with Goodman furnace. Upon inspection, discovered extensive rodent infestation inside unit with nesting material throughout components. Internal examination revealed severe rusting and seized components due to previous basement flooding approximately six years ago. Multiple mice were observed within the heat exchanger area. After consultation with homeowner and demonstrating the extent of damage, recommended full system replacement as repairs would likely approach replacement cost. Responded to no heat call at property with Goodman furnace. Upon inspection, discovered extensive rodent infestation inside unit with nesting material throughout components. Internal examination revealed severe rusting and seized components due to previous basement flooding approximately six years ago. Multiple mice were observed within the heat exchanger area. After consultation with homeowner and demonstrating the extent of damage, recommended full system replacement as repairs would likely approach replacement cost.

Shawn G.

Shawn G. Job Checkin

Replaced broken shower arm after removing threaded portion that was stuck in the wall. Removed access panel to replace damaged 90-degree copper fitting, then installed new winged 90 and reattached shower arm to restore functionality.

Replaced broken shower arm after removing threaded portion that was stuck in the wall. Removed access panel to replace damaged 90-degree copper fitting, then installed new winged 90 and reattached shower arm to restore functionality. Replaced broken shower arm after removing threaded portion that was stuck in the wall. Removed access panel to replace damaged 90-degree copper fitting, then installed new winged 90 and reattached shower arm to restore functionality.

Mike B.

Mike B. Job Checkin

Performed comprehensive inspection of heating systems at commercial property, focusing on boiler floor heat systems in North barn and equipment in big shop area. Verified operation of all circulation pumps in both areas and conducted full diagnostics on boiler systems. Identified faulty flame sensors and spark rods requiring replacement on both boilers. Submitted parts requisition form to obtain necessary replacement components.

Performed comprehensive inspection of heating systems at commercial property, focusing on boiler floor heat systems in North barn and equipment in big shop area. Verified operation of all circulation pumps in both areas and conducted full diagnostics on boiler systems. Identified faulty flame sensors and spark rods requiring replacement on both boilers. Submitted parts requisition form to obtain necessary replacement components. Performed comprehensive inspection of heating systems at commercial property, focusing on boiler floor heat systems in North barn and equipment in big shop area. Verified operation of all circulation pumps in both areas and conducted full diagnostics on boiler systems. Identified faulty flame sensors and spark rods requiring replacement on both boilers. Submitted parts requisition form to obtain necessary replacement components.

Trent L.

Trent L. Job Checkin

Responded to no heat service call on aging Lennox furnace. Diagnostic inspection revealed inducer motor was operational but ignition sequence was failing due to completely plugged pressure switch. Cleaned pressure switch, serviced flame sensor, and verified proper component operation. System now functioning correctly, but documented significant rust deterioration on burners with photos. Customer will receive estimate for burner replacement as recommended preventative maintenance.

Responded to no heat service call on aging Lennox furnace. Diagnostic inspection revealed inducer motor was operational but ignition sequence was failing due to completely plugged pressure switch. Cleaned pressure switch, serviced flame sensor, and verified proper component operation. System now functioning correctly, but documented significant rust deterioration on burners with photos. Customer will receive estimate for burner replacement as recommended preventative maintenance. Responded to no heat service call on aging Lennox furnace. Diagnostic inspection revealed inducer motor was operational but ignition sequence was failing due to completely plugged pressure switch. Cleaned pressure switch, serviced flame sensor, and verified proper component operation. System now functioning correctly, but documented significant rust deterioration on burners with photos. Customer will receive estimate for burner replacement as recommended preventative maintenance.

Gary L.

Gary L. Job Checkin

Diagnosed intermittent heating failure on 21-year-old Gibson furnace. Inspection revealed dirty flame sensor and burners affecting system operation, with questionable heat exchanger condition. Performed flame sensor cleaning to restore temporary operation and scheduled comfort advisor for comprehensive system evaluation due to age and condition of unit.

Diagnosed intermittent heating failure on 21-year-old Gibson furnace. Inspection revealed dirty flame sensor and burners affecting system operation, with questionable heat exchanger condition. Performed flame sensor cleaning to restore temporary operation and scheduled comfort advisor for comprehensive system evaluation due to age and condition of unit. Diagnosed intermittent heating failure on 21-year-old Gibson furnace. Inspection revealed dirty flame sensor and burners affecting system operation, with questionable heat exchanger condition. Performed flame sensor cleaning to restore temporary operation and scheduled comfort advisor for comprehensive system evaluation due to age and condition of unit.

Gary L.

Gary L. Job Checkin

Diagnosed and corrected an electrical issue affecting the heating system, which occurred after previous electrical work performed by Bear Valley electrical company. Found reversed polarity on furnace wiring and corrected the connections to ensure proper operation. System is now functioning normally with all electrical connections properly terminated.

Diagnosed and corrected an electrical issue affecting the heating system, which occurred after previous electrical work performed by Bear Valley electrical company. Found reversed polarity on furnace wiring and corrected the connections to ensure proper operation. System is now functioning normally with all electrical connections properly terminated. Diagnosed and corrected an electrical issue affecting the heating system, which occurred after previous electrical work performed by Bear Valley electrical company. Found reversed polarity on furnace wiring and corrected the connections to ensure proper operation. System is now functioning normally with all electrical connections properly terminated.

Beca R.

Beca R. Job Checkin

Responded to no-heat call for 20-year-old system with combustion error indication (green flashing light). Diagnostic testing revealed inducer motor locked up, preventing proper furnace ignition. Attempted to free the seized inducer motor but was unsuccessful. Created estimate for inducer replacement and scheduled follow-up appointment for complete furnace replacement due to system age and condition.

Responded to no-heat call for 20-year-old system with combustion error indication (green flashing light). Diagnostic testing revealed inducer motor locked up, preventing proper furnace ignition. Attempted to free the seized inducer motor but was unsuccessful. Created estimate for inducer replacement and scheduled follow-up appointment for complete furnace replacement due to system age and condition. Responded to no-heat call for 20-year-old system with combustion error indication (green flashing light). Diagnostic testing revealed inducer motor locked up, preventing proper furnace ignition. Attempted to free the seized inducer motor but was unsuccessful. Created estimate for inducer replacement and scheduled follow-up appointment for complete furnace replacement due to system age and condition.

Trevor P.

Trevor P. Job Checkin

Performed scheduled maintenance on oil-fired Wheel Mclain boiler with Beckett burner assembly. Conducted inspection of system components and documented equipment specifications including 85-45B designation. Unable to complete full tune-up due to lacking correct replacement nozzle; customer approved parts order for future installation and signed corresponding documentation.

Performed scheduled maintenance on oil-fired Wheel Mclain boiler with Beckett burner assembly. Conducted inspection of system components and documented equipment specifications including 85-45B designation. Unable to complete full tune-up due to lacking correct replacement nozzle; customer approved parts order for future installation and signed corresponding documentation. Performed scheduled maintenance on oil-fired Wheel Mclain boiler with Beckett burner assembly. Conducted inspection of system components and documented equipment specifications including 85-45B designation. Unable to complete full tune-up due to lacking correct replacement nozzle; customer approved parts order for future installation and signed corresponding documentation.

Trent L.

Trent L. Job Checkin

Responded to no-heat service call on a 15-year-old furnace that was only running for 20-30 minutes before shutting down. Diagnostic inspection revealed flames rolling out and tripping the rollout switch, with visible cracks in the heat exchanger near the inlet and on at least one primary cell. Found burner tubes completely plugged with soot, likely caused by incorrect gas pressure or partial exhaust blockage. Recommended replacement options for heat exchanger and complete furnace/AC system, with follow-up appointment scheduled.

Responded to no-heat service call on a 15-year-old furnace that was only running for 20-30 minutes before shutting down. Diagnostic inspection revealed flames rolling out and tripping the rollout switch, with visible cracks in the heat exchanger near the inlet and on at least one primary cell. Found burner tubes completely plugged with soot, likely caused by incorrect gas pressure or partial exhaust blockage. Recommended replacement options for heat exchanger and complete furnace/AC system, with follow-up appointment scheduled. Responded to no-heat service call on a 15-year-old furnace that was only running for 20-30 minutes before shutting down. Diagnostic inspection revealed flames rolling out and tripping the rollout switch, with visible cracks in the heat exchanger near the inlet and on at least one primary cell. Found burner tubes completely plugged with soot, likely caused by incorrect gas pressure or partial exhaust blockage. Recommended replacement options for heat exchanger and complete furnace/AC system, with follow-up appointment scheduled.

Shawn G.

Shawn G. Job Checkin

Diagnosed issue with recirculation pump not providing hot water. Determined that ball valves to recirculation lines were in closed position. Opened valves and confirmed proper operation of recently installed circulation pump. System now functioning correctly with adequate hot water flow.

Diagnosed issue with recirculation pump not providing hot water. Determined that ball valves to recirculation lines were in closed position. Opened valves and confirmed proper operation of recently installed circulation pump. System now functioning correctly with adequate hot water flow.

Ben W.

Ben W. Job Checkin

Responded to no heat complaint on Comfortmaker EnviroPlus 90 furnace. Diagnosed dirty flame sensor preventing main burners from igniting despite pilot flame. Removed and cleaned flame sensor, restoring ignition. Noted significant rust on burners causing pronounced ignition flash. Identified secondary heat exchanger leak and inducer motor leaking at seam. Performed visual inspection of heat exchanger by removing blower. Recommended replacement of burners, inducer motor, and heat exchanger. Service advisor scheduled for follow-up.

Responded to no heat complaint on Comfortmaker EnviroPlus 90 furnace. Diagnosed dirty flame sensor preventing main burners from igniting despite pilot flame. Removed and cleaned flame sensor, restoring ignition. Noted significant rust on burners causing pronounced ignition flash. Identified secondary heat exchanger leak and inducer motor leaking at seam. Performed visual inspection of heat exchanger by removing blower. Recommended replacement of burners, inducer motor, and heat exchanger. Service advisor scheduled for follow-up. Responded to no heat complaint on Comfortmaker EnviroPlus 90 furnace. Diagnosed dirty flame sensor preventing main burners from igniting despite pilot flame. Removed and cleaned flame sensor, restoring ignition. Noted significant rust on burners causing pronounced ignition flash. Identified secondary heat exchanger leak and inducer motor leaking at seam. Performed visual inspection of heat exchanger by removing blower. Recommended replacement of burners, inducer motor, and heat exchanger. Service advisor scheduled for follow-up.

Ben W.

Ben W. Job Checkin

Responded to no heat call and identified rollout switch tripped due to clogged filter. Installed new air filter and reset rollout switch, which temporarily restored furnace operation. Upon inspection, discovered perforations in the heat exchanger at the primary header junction and heavily rusted burners. Tagged equipment as unsafe and scheduled service advisor consultation to discuss heat exchanger and burner replacement options.

Responded to no heat call and identified rollout switch tripped due to clogged filter. Installed new air filter and reset rollout switch, which temporarily restored furnace operation. Upon inspection, discovered perforations in the heat exchanger at the primary header junction and heavily rusted burners. Tagged equipment as unsafe and scheduled service advisor consultation to discuss heat exchanger and burner replacement options. Responded to no heat call and identified rollout switch tripped due to clogged filter. Installed new air filter and reset rollout switch, which temporarily restored furnace operation. Upon inspection, discovered perforations in the heat exchanger at the primary header junction and heavily rusted burners. Tagged equipment as unsafe and scheduled service advisor consultation to discuss heat exchanger and burner replacement options.

Doug T.

Doug T. Job Checkin

Repaired multiple burst copper pipe sections in utility area of tiny house. Identified three separate compromised joints requiring repair work. Successfully replaced and reconnected all damaged sections, restoring proper function to the plumbing system.

Repaired multiple burst copper pipe sections in utility area of tiny house. Identified three separate compromised joints requiring repair work. Successfully replaced and reconnected all damaged sections, restoring proper function to the plumbing system. Repaired multiple burst copper pipe sections in utility area of tiny house. Identified three separate compromised joints requiring repair work. Successfully replaced and reconnected all damaged sections, restoring proper function to the plumbing system.

Doug T.

Doug T. Job Checkin

Diagnosed Navien tankless water heater (approximately 7-8 years old) exhibiting no hot water condition with error code E001. After inspection of internal components, determined main pump and motherboard failure. Presented customer with options for complete unit replacement with new Navion model or component repair service.

Diagnosed Navien tankless water heater (approximately 7-8 years old) exhibiting no hot water condition with error code E001. After inspection of internal components, determined main pump and motherboard failure. Presented customer with options for complete unit replacement with new Navion model or component repair service. Diagnosed Navien tankless water heater (approximately 7-8 years old) exhibiting no hot water condition with error code E001. After inspection of internal components, determined main pump and motherboard failure. Presented customer with options for complete unit replacement with new Navion model or component repair service.

Bryson E.

Bryson E. Job Checkin

Diagnosed multiple leak issues in water heater system, including temperature and pressure (T&P) valve, recirculation pump, and pressure tank. Provided customer with estimate for replacement of T&P valve, recirculation pump, and pressure tank to resolve all leaking components.

Diagnosed multiple leak issues in water heater system, including temperature and pressure (T&P) valve, recirculation pump, and pressure tank. Provided customer with estimate for replacement of T&P valve, recirculation pump, and pressure tank to resolve all leaking components. Diagnosed multiple leak issues in water heater system, including temperature and pressure (T&P) valve, recirculation pump, and pressure tank. Provided customer with estimate for replacement of T&P valve, recirculation pump, and pressure tank to resolve all leaking components.